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SERVICEMAN’S LOG
Turning a pile of junk into computers
Bruce Pierson of Dundathu, Queensland,
repairs many laptop/notebook
computers. He often gets them
inexpensively (or even for free) because
they’re broken, then uses parts from
one to fix another. Here are several
stories of computers he’s fixed lately...
I have a few old laptops that I have installed various
versions of Linux on to try out. Among these is a Compaq
CQ60 that was my younger daughter’s first laptop. The last
time I looked at it, it had a stuck key, causing it to beep
continuously while on. Fixing that would require replacing the keyboard.
I got it out recently and looked through my box of keyboards that I had salvaged from old laptops over time. I still
did not have a keyboard that would suit this laptop and
was reluctant to spend $25 to buy a new one for a device
I’m not using.
I then noticed that one corner of the keyboard surround
near the screen was sticking up. I checked under the laptop
and the screw was in place, so something must have broken inside. I removed the screws on the bottom that held
the keyboard surround on and found that the brass nut had
broken out of the post in the corner that was sticking up.
I considered how I could repair this part. I decided to
get out my 40W soldering iron to heat the brass nut and
press it into the now shorter post. That worked, and I put
the screw in to make sure it sat vertically. A bit more heat
allowed me to true it up. Now I would need a longer screw
for this corner.
I looked through my laptop screws but I had nothing longer than the original screw. Then I remembered that several years ago, someone had given me a small
parts cabinet with around 30 small drawers
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in it. I looked through the drawers; most of the parts were
for PCs, but I found some laptop screws. They were mainly
short, but in another drawer, I found one that was exactly
the right length.
I refitted the keyboard surround, but when I went to use
the replacement screw, I discovered that the head was a
larger diameter and it would not fit in the hole. So I put the
screw in my small electric drill and, with the drill running,
I used a file to reduce the diameter of the head, checking it
periodically against the original screw to get the diameter
approximately the same.
With the screw modified, I was able to install it and now
the keyboard surround is fitting correctly. Now I just need
a good keyboard to get it back in working order.
Toshiba C50D-A screen replacement
Recently, a friend asked me if I could have a look at his
Toshiba laptop. It had a round ‘black hole’ in the screen
that was becoming increasingly annoying. The laptop was
fine apart from this. I have seen some weird things with
faulty screens in the past, but this is the first time I’ve seen
one with a black hole.
The cost of a new screen was over $90, so he wondered if
I might have a good screen from an old laptop that would fit
his. As it happened, I had recently disassembled a Toshiba
L650 laptop that no longer worked, and I still had the shell
and screen sitting on a shelf. I did some online research
and found that both laptops use exactly the same screen.
I started by removing the battery, then the RAM and
HDD cover, and I took out the hard drive and RAM. Then
I removed the optical drive plus the 15 screws securing the
back shell, allowing me to remove the back shell.
Australia's electronics magazine
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Items Covered This Month
• A tale of four computers
• Repairing a Hisense 65U8G power board
• A faulty IR sensor in a carport
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
This laptop is very unusual in that the bottom shell comes
off, leaving the motherboard in the top panel, whereas with
most laptops, the top panel comes off, leaving the motherboard in the bottom shell.
I could see that I would need to remove the motherboard to detach the cable going to the screen. This meant
removing the keyboard. That turned out to be a nightmare
with the way the keyboard is fitted into the top panel, but
I finally got it out and unplugged the cable.
Next, I removed the CPU fan and I was surprised by the
amount of junk that was almost entirely blocking the fins
on the heatsink. It’s a wonder the laptop had not been overheating; it was one of the worst I’ve seen.
I unplugged all the plugs in various locations around
the motherboard, then removed the single screw from the
motherboard and lifted it up to unplug the video cable.
After removing the motherboard, I cleared the rubbish
off the heatsink and cleaned the small amount of dust off
the fan.
After removing the last two screws from each of the
hinges, I had the lid with the screen free. Removing the two
screws in the bottom front corners of the screen allowed
me to prise the inner surround free from the lid.
Then I noticed a problem. On one lower corner of the
lid, the two small brass nuts had come out due to the old
plastic becoming brittle over time and breaking.
There was no easy way to remedy this situation. There
would be no way to secure the hinge on that side to the lid
without coming up with a solution. I did not have a spare
lid for this laptop.
My friend asked me what I could do to get the repair
completed, as this laptop was very useful to him. I said
I could put two screws through the lid from the back to
secure the hinge, but that he would see the screws in the
back of the lid. He said that he wasn’t concerned how the
lid looked from the back.
So I got the screen from the L650, unplugged the cable
from it and removed the hinges. Then I did the same with
the original screen and I fitted the original hinges and original cable to the replacement screen.
With the screen re-fitted to the lid, I lined things up,
drilled the two holes through the lid and then lightly countersunk them on the outside of the lid. I had to find two
small screws and nuts that were long enough to do the job.
This is not easy, as laptop screws do not commonly come
that long. But with some searching through my containers
of laptop screws, I found two suitable ones.
I used the two small brass nuts that had come loose from
the lid to fit the screws in the lid. This ensured that the
hinges were in the correct place. I eventually found two tiny
nuts to finish the repair. I fitted one to the screw through
the hinge, then I replaced the surround and screwed the
last nut onto the screw in the corner of the screen.
The very dirty Toshiba
C50D.
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May 2026 99
I could now reassemble the laptop. I fitted the two screws
to each hinge to hold the lid onto the laptop, then I connected the screen cable to the motherboard and sat the
motherboard back in place. I screwed in the single screw
that holds it to the top panel.
I connected the rest of the cables to the motherboard,
then put the CPU fan in place and installed the two screws
that hold it to the motherboard, and plugged in its cable. I
sat the back shell in place so I could turn the laptop over
and connect the keyboard.
I plugged in the keyboard cable, then I had a lot of trouble getting the keyboard back in place. I have never had
this much trouble removing and refitting a keyboard on
any other laptop previously. But I got it correctly fitted
in the end.
I closed the lid, turned the laptop back over and screwed
the back shell on. Then I fitted the hard drive, RAM and
optical drive. I replaced the cover for the hard drive and
RAM, and installed the battery.
I tested the laptop and everything was good with it now.
I gave the keyboard a quick clean. My friend was really
happy to see his laptop nice and clean, no longer with a
hole in the screen.
While it may not have been a cosmetically perfect repair,
at least it saved the laptop from being scrapped.
HP 15 Notebook RAM upgrade
I wanted to try Windows 11 so, using a Windows 10 laptop, I downloaded the Windows 11 25H2 ISO file and used
Rufus to copy it to a 16GB flash drive.
I had an unused HP laptop but it won’t boot from a flash
drive, like many later PCs will, so I had to run the setup
from inside Windows 10. This laptop had no personal
information on it, so I just wiped everything and started
fresh with Windows 11.
The installation went smoothly until I got to connecting
to the internet. I knew that if I connected to the internet,
that I would have to log in with a Microsoft account, which
I did not want to do, as it would be a massive inconvenience to need internet access every time I wanted to log
into Windows.
I got to a command prompt by holding Shift and pressing F10, and I entered the command “oobe\bypassnro”.
This initiated a reboot, and it then showed “I don’t have
internet”, so I could log in with a local account, just like
in Windows 10.
At the Windows 11 desktop, the first thing I noticed
was that the start button was in the middle of the taskbar,
which was impractical. I found the setting and changed it
back to where it should be. Then I found that many of the
usual features were missing from the taskbar.
I did some searching online and I found a way to fix this.
I found Explorer Patcher and tried to download it using
Microsoft Edge, but it would not complete the download,
stopping before it was completed. So I downloaded and
installed Google Chrome and then I was able to download
Explorer Patcher and run it. That fixed the taskbar and I
was then able to put Quick Launch back on it.
This HP laptop only had 4GB of RAM, which is very low
for Windows 11. I wanted to upgrade the RAM to 8GB. This
HP laptop is one of those laptops that must be completely
dismantled to replace the RAM or change the hard drive,
which makes upgrading or changing anything difficult.
With the top panel removed, I had to remove the motherboard to find the RAM. At this point, I was becoming
concerned that the RAM might be soldered to the motherboard and not be upgradeable, as I’ve found this on some
laptops previously. But after removing the motherboard, I
found that there was a single 4GB RAM module in a slot,
so it could be upgraded, unlike the soldered CPU.
Now I needed an 8GB RAM module. I still had several
old, non-working laptops, so I started by checking all the
The HP 15 motherboard; the RAM is next to the CMOS cell.
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HP laptops, but I did not find any 8GB RAM modules. Then
I also checked other brands of non-working laptops and I
removed several hard drives and RAM modules, but I still
had no 8GB RAM module.
Then I found an Asus F553M laptop that was another
one of these laptops that needs to be completely dismantled to access anything. I dismantled it and it had one 8GB
RAM module.
I got my Dell laptop that has Linux on it and I removed
the two 4GB RAM modules and installed the single 8GB
RAM module. Running MemTest86+, it went through the
entire test with no errors, so I knew that I had a good 8GB
RAM module.
I then installed the 8GB RAM module in the HP laptop.
Next, I decided to check the CR2032 cell to see what condition it was in. I first tested it with my multimeter and it
read 2.97V, a sure indication that it had reached the end
of its life. I got out my dedicated cell and battery tester
and checked the cell and it read 1V, 0%, so it needed to
be replaced.
The new cell measured 3.2V and 100%, so I fitted it
to the laptop motherboard. It’s always a good idea to test
replacement cells to make sure they are still good, as some
cells may be getting old and losing their voltage, which
happens over time, even when a cell is not being used.
Some laptops have the CMOS battery (cell) located in a
convenient location under one of the covers, usually the
RAM cover. But a lot of laptops have it in a location that
is not visible, and it’s necessary to dismantle the laptop in
order to replace the cell.
Some laptops even have the cell soldered to the motherboard, but these are mostly rechargeable cells and they
don’t normally need replacing for the life of the laptop.
With the laptop reassembled, I could see that the battery had started charging after sitting on 0% for some time
while I had been using it. Laptop batteries that have been
sitting around for a long time will usually go flat. Often
they will not charge up again, but in some cases they will
come good if left on charge for a long time.
I ran msinfo32, which brought up the specifications for
the laptop. This is a very handy command for finding out
just what’s inside a laptop, as it shows the CPU, hard drive,
RAM and many other details.
Compaq CQ42 CPU upgrade
I was setting up a Compaq CQ42 to run Linux when I
found that the CMOS battery (cell) was flat. It would be a
big job to change the cell, as the laptop would need to be
completely dismantled and the motherboard removed to
access the cell.
Unfortunately, this is another of that frustrating class of
portable computers that has the CMOS cell mounted in an
inaccessible place. So once again, I’d have to totally dismantle it to complete the swap.
Seeing that I would have to go a lot of trouble just to
replace the cell, I thought I would upgrade the CPU while
I had it apart. It had a Celeron T3100 at 1.90GHz; I had
some spare CPUs that I’d salvaged from dead and defective laptops.
I started by searching through the CPUs that had the
same socket (PGA478). I set aside any processor that was
faster than 2GHz – I had four. Next, I checked which CPUs
were compatible with the CQ42 motherboard. I found the
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May 2026 101
I figured that while replacing the CR2032 cell in this Compaq CQ42 laptop, I could also replace the CPU,
best option to be a Pentium dual-core P4500 at 2.3GHz, as
it was listed as the most common CPU in the CQ42. I had
a faster 2.4GHz CPU but it was not compatible.
The first step was to remove the battery and the cover
for the hard drive, then the cover for the RAM. Next, I
removed the optical drive. I first opened it with an optical
drive eject tool so that I could pull on the tray and not the
front panel. Then I removed the WiFi card after removing
the mounting screw and unplugging the two wires.
Next, I removed the three screws holding in the hard
drive and unplugged the connector. Most hard drives are
not held in with screws like this one.
Many laptop keyboards are held in with small clips at
the top or bottom of the keyboard, or occasionally screws
at the top of the keyboard that are accessible after removing
a panel. The CQ42 is quite different in that the keyboard
is held in by six screws from the underside.
I removed the six screws and then used the optical drive
eject tool to push up on the keyboard through one of the
screw holes.
This allowed me to lift up the keyboard, disconnect
the cable and lift the keyboard clear. I then removed the
remaining screws on the bottom of the laptop and the one
screw under the keyboard, unplugged the four cables and
prised the top panel off.
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
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Please be sure to include your full name and address details.
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Silicon Chip
After removing one screw holding in the CPU cooling fan
and two holding in the motherboard, I unplugged all the
cables and lifted out the motherboard. I could then unscrew
the six screws holding the heatsink and fan to it and remove
the heatsink with the fan still attached to it. Then I cleaned
the old heatsink compound off the CPU heatsink.
I fired up the compressor and blew compressed air
through the fins of the heatsink. Quite a lot of junk
came out, so it was definitely in need of cleaning. I also
cleaned the fan’s fins with a damp, squashed cotton bud
so that the assembly would be ready to refit after changing the CPU.
I changed the CPU, applied new heatsink compound
and reinstalled the heatsink. Then I changed the CMOS
battery (cell), which was the main reason for completely
dismantling the laptop. With that done, it was time to
reassemble it.
I put the motherboard back in the bottom shell and
installed the two screws to hold it in and the one screw
to hold in the CPU cooling fan. Next, I reconnected all
the cables, put the top panel back in place and connected
the four cables that were in the top shell. I installed the
one screw in the top shell and all the screws in the bottom shell.
I then plugged in the keyboard cable, put the keyboard in
place and reinstalled the six screws from the bottom. After
reinstalling the WiFi card and connecting its two wires, I
refitted the optical drive and installed the screw that holds
it in place. Then I plugged in the hard drive connector,
sat the hard drive in place and drove in the three screws.
I put the hard drive cover on, installed one 2GB RAM
module and put the battery back in.
The battery was not charged, so I connected a charger
and pressed the power button. I tapped the Esc key and
then I pressed the F10 key to access the BIOS setup. I set
the time and date, then checked the other settings before
exiting setup and saving the new settings.
Now that I was ready to install the operating system, I
switched it off, inserted the other 2GB RAM module and
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put the RAM cover back on. I considered upgrading the
RAM to 8GB, but I decided not to, as Linux is pretty light
on RAM usage and I would only be using it for web surfing and research.
I had already set the laptop to boot from the optical drive
as the first choice, so I booted from the PearOS Monterey
installation DVD. Installing Linux on these old laptops
gives them a new lease on life. It can fit on a 40GB hard
drive, but I usually use 120GB or larger.
Hisense 65U8G power board repair
This LCD TV has a dimmable LED backlight, using more
power than a normal LCD TV with a simple backlight. The
advantage is higher contrast (stronger blacks). An LCD panel
does not fully block the backlight, so the blacks appear dark
grey. By selectively switching off the backlight elements,
the blacks are more black.
In the future, RGB panels, with a matrix of red, blue, and
green LEDs, promise to provide a high-contrast screen better than OLED TVs.
The power board in this TV has a power factor correction (PFC) stage using an IPD2308 IC that makes its current draw more sinusoidal, in phase with the mains voltage waveform.
The normal capacitor input supplies used in LCD TVs
take large spikes of current at the peak of the mains voltage
and are not popular with supply companies.
This PFC circuit is unusual in that it uses two transformers, each driven by a separate input Mosfet, although both
Mosfets are driven by the same IDP2308 chip. I think this
is done because it’s easier to fit two smaller transformers
than one large one. The outputs of the two transformers are
connected so that only one Mosfet half-bridge is required
on the output side.
The power fuse to the board was blown, and both the
input Mosfets were shorted. The input Mosfets share the
same 0.05W current-sensing resistor (3 × 0.15W in parallel). These were blown open. The circuits driving the input
Mosfets were damaged as the Mosfets shorted, and the
IPD2308 was also destroyed.
Each Mosfet had a PNP emitter-follower transistor to
speed up its switch-off. Surprisingly, the PNP transistors
survived, but two resistors in each driving circuit were
open-circuit.
So quite a few components to replace. As the IC and
resistors are surface mount, you need a hot air gun for
the IC and hot tweezers for the resistors. So you have to
decide whether to repair or buy a second-hand board on
eBay or similar.
Roger Sanderson, Sinnamon Park, Qld.
IR motion sensor repair
We have a sensor in our carport looking at the driveway to
detect visitors as they enter the property. This is necessary
as the driveway is not easily seen from inside the house.
The sensor is a simple infrared motion detector (transmitter) with a separate light/beeper box (receiver) to provide
an indication of activity in the driveway.
The units are connected wirelessly and run off batteries that seem to last forever. I bought the unit from Altronics, and it has proved reliable and just the right solution
for the job.
After many years of flawless service, the unit developed
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an intermittent fault. The lights in the receiver would flash
when triggered, but the audible alarm would not sound.
As the beeper unit normally sits on the hall table where it
can’t be readily seen, this was a problem.
I assumed the transmitter unit was working correctly.
I duly inspected the receiver unit, replaced the batteries,
and the beeper came back to life. Good! The unit was put
back into service and continued its duties until the beeper
failed again several months later.
This time, I took the back off the receiver and gave it a
thorough inspection. It was a fairly simple construction, a
main printed circuit board with a small wireless receiver
board soldered to its side. Nothing was obviously amiss.
I touched up a few possibly cold solder joints, but still no
sound.
Checking the loudspeaker, I found it was fine, measuring 95W and producing a healthy click each time the meter
probes were attached. I removed a transistor that seemed
to switch the input to the audio circuits and tested it, but
it was reported as working correctly, so I returned it to
the circuit.
Various other components were checked in-circuit with
nothing obvious showing up. Fortunately, most of the components were marked with their values, and that allowed
easy checking.
As I worked through these components, it came to the
point where a small IC on the board was the only untested
component in the beeper circuit. I could not figure out what
it actually did; it had an obscure part number that failed
to show up in web searches.
At that point, I decided it was time to give up and look
for a replacement driveway detector. After much looking
around at various modern equivalents that had up to 50
tones, pushbuttons galore, connecting to my phone and
everything else I did not want, I found Altronics were still
selling the original unit and duly ordered a new one.
While waiting for the new unit, I could not leave the
thought alone that it was a simple unit, the fault had to be
in the beeper circuitry, and I could not allow myself to be
defeated! So instead of tidying up my bench and sweeping
the faulty unit into the bin, I had another look.
Having eliminated all the likely components around the
beeper circuit, I realised that the beeper had two sound
levels that were controlled by a two-pole, three-position
slide switch located on the other side of the board. The
switch doubled as the on/off switch and was connected to
the beeper circuit by two tracks that meandered across the
board, avoiding other tracks and components.
Testing the switch contacts, I quickly found that
they were either open-circuit or had a high resistance.
I bridged out the switch, and the beeper came to life! I
decided that as we only ever used the unit on low volume, it was easier to leave the switch bridged than find
a replacement. The on/off side of the switch seemed to
be working fine.
With 20/20 hindsight, I realised that in circuits such
as these where there is little loading of parts, and barring
a random component failure, the most likely component
to fail is the one subject to mechanical wear. So I probably should have looked at the switch first. The unit was
returned to service, and I now have a brand new unit sitting on my shelf as a backup!
SC
Nigel Dudley, Ocean Beach, WA.
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