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Vintage Radio
RCA Radiola 17 (AR-927) radio
from 1927
The Radiola 17
is an interesting
seven-valve ACpowered tuned
radio frequency
(TRF) set from 1927.
By Jim Greig
T
he Radiola 17’s price on release
was US$157.50 with valves, equivalent to around US$2900 or $4450
today.
A TRF radio comprises one or more
tuned RF amplifier stages in series.
Each stage includes a bandpass filter
tuned to the same frequency, which
amplifies the desired signal while
attenuating others. After several
stages, the selected signal is significantly amplified, while out-of-band
signals are progressively filtered out.
The earliest such sets had individual
tuning capacitors for each stage, making tuning to a station an art. By 1927,
the use of a ganged tuning capacitor
meant that only a single tuning knob
was required.
Radios were operated almost exclusively from batteries until around
1925. Early battery sets used directly
heated valves, where the filament also
served as the cathode. Later designs
introduced indirectly heated valves
with separate filaments and cathodes,
solving several technical problems.
One minor problem was uneven
voltage distribution, both along the
length of the filament in a single valve,
and between the filaments of different
valves. A more serious problem arose
when sets began using mains power:
if the filament also acted as the cathode, powering it with AC introduced
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significant hum. Various methods were
developed to minimise this, including:
1. Using DC for the filament supply.
This often meant using a battery in the
1920s, as high-current, low-
voltage
rectifiers were not yet available.
2. Centre-tapped hum-balancing
potentiometers. A pot across the filament with its centre tap grounded
made the ends of the filament equal
and opposite in phase, helping to cancel the hum.
3. Special filament coatings. These
may have reduced temperature variation along the filament over the AC
cycle.
4. Lower filament voltages. Any AC
ripple imposed on the signal would
be less than it would be with a higher
voltage.
5. Separating the cathode and filament. The filament then acted purely
as a heater, with the cathode isolated
electrically, eliminating the main
source of hum.
The first AC-powered set may have
been the Rogers Batteryless from Canada. Rogers designed and produced
their own AC valves (type 32) with a
separate cathode. Powering the radio
from AC saved the costs of batteries,
making radio accessible to many more
people.
In 1927, RCA introduced a new tube,
the UX-226 (also known as the type 226
Australia's electronics magazine
or type 26), a
triode that could be
used for any stage of a receiver except
the detector (unless the designer was
willing to accept inferior performance).
It had a low-voltage (1.5V) coated filament that was optimised to produce
very little hum when run on AC power.
The same year, RCA announced the
UY-227. The type 27 had the same
shape as the type 26, but its filament
was arranged to heat an oxide-plated
cathode connected to a fifth pin in the
base. Its filament was isolated from
the electron path, and the new tube
made an excellent detector (or audio
amplifier).
The RCA 17 was RCA’s first AC-
powered receiver, and it uses the following valve types: UX226 (first RF),
UX226 (second RF), UX226 (third
RF), UY227 (detector), UX226 (audio
preamp), UX171 (audio output) and
UX280 (mains rectifier).
Circuit details
Much of the following information
was derived from the RCA Service
Notes and Service Data.
The main part of the circuit, shown
in Fig.1, is deceptively simple. The
first RF stage is untuned, with the
antenna connected to the grid through
the volume control. Unlike in early
battery sets, where the volume was
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Fig.1: at first glance, the RCA Radiola 17 circuit seems to be little more than seven valves connected in series with coupling transformers, some with tuning.
often controlled by varying filament
voltage, AC-powered sets required a
different method.
In this case, the volume control is
simple but effective: a potentiometer
in series with the antenna provides
adjustable attenuation of the incoming RF signal before it reaches the first
RF amplifier.
The second and third stages are
tuned RF triodes. The triode has significant anode-to-grid capacitance,
and this, multiplied by the gain (Miller
Effect), results in capacitances of tens
of picofarads. A triode RF amplifier
with high-Q tuned circuits at the grid
and anode is especially susceptible to
parasitic oscillation. Something must
be done to ensure stability.
This may be:
1. Neutralisation. Feed back an outof-phase signal from the anode circuit
through a carefully selected capacitor
to the grid. This was subject to a patent
by the Hazeltine Company.
2. Including a resistor, often in the
tuned circuits, to reduce the Q. However, Don Sutherland argues it is the
phasing of transformers and the layout
that have the most effect.
In this radio, the coils are all at
right-angles to reduce mutual coupling
and improve stability. There is also a
resistance (800W in the circuit, but my
resistors were actually 1kW) added in
series with the grids. There is a section
in the Service Notes on “Uncontrolled
Oscillation”, with a number of possible remedies, including dropping the
filament voltage (and therefore gain)
of the type 26 valves.
The third stage is coupled to the
grid-leak detector through a mica
capacitor of around 150pF. A gridleak resistor bleeds off any charge
that might accumulate on the grid
from rectification of the incoming RF
signal, preventing charge build-up
and allowing the grid to operate at a
slightly negative voltage.
In a grid leak detector, the grid/
cathode of the tube acts as a rectifier,
albeit an inefficient one. While the grid
voltage to plate current transfer relationship may not be perfectly linear,
non-linearity is not required for detection, unlike in an anode bend detector.
The RF is filtered off at the plate, and
only the average voltage remains; the
audio interstage transformer does this
from its limited bandwidth and any
residual RF is filtered out by the capacitor in parallel with the transformer
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March 2026 93
Fig.2: the power supply circuit is similarly quite simple. The connector strip on the left corresponds to the one on the right in Fig.1. That’s how they are
physically connected in the radio.
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output. If no audio interstage transformer is used, the RF can be removed
by a capacitor in combination with
the valve’s anode resistor and its plate
resistance.
The rectified signal is fed via an
audio transformer to the first AF stage.
Its output is transformer-coupled to the
output stage, which has a 1:1 transformer to the speaker.
AF transformers were used in early
radio for coupling as the valves had
little gain, and the (typically) 1:3 voltage ratio offered by a transformer was
basically free (sometimes capacitive
coupling was used too). The amplification factor of the type 26 is around
eight times; the two audio transformers
add another nine times, or as much as
an additional 26 valve.
Today, the amplification factor of
a 12AX7 (for example) is around 100
times, and the losses from RC-coupling
a 12AX7 are easily covered. The transformers are just two windings with
no interleaving and minimal iron,
resulting in high leakage inductance
and limited bandwidth, limiting this
radio’s audio frequency range.
The expected loudspeaker response
at the time was also limited, so this
was not a concern.
Audio transformer properties
Audio interstage transformers in
vintage radios are special parts; they
cannot be analysed with the usual
equations for a transformer because no
power is transferred. The grid of the
following stage (operating in Class-A)
draws no significant current. The analysis that applies to them is that of a
damped, coupled resonant circuit.
The damping is provided by the
anode resistance of the valve driving the transformer. The resonant
frequency is defined mainly by the
self-capacitance of the secondary
winding, with contributions from the
primary. The mutual inductance (and
therefore leakage inductance) is very
important in the balance of factors
that result in a flat frequency response.
When the manufacturer gets the
balance of factors just right, the transformer behaves as an astonishingly
effective bandpass filter in the audio
spectrum, with a flat response. They
should always be preserved where
possible. Their band-pass response
typically extends from as low as
100Hz, up to around 7-10kHz.
They provide improved dynamic
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range compared to anode resistor loads
as they hold the anode voltage closer
to the B+ voltage. They can provide
passive voltage amplification up to
around three times, or at high as five
times; the higher the gain, the more
difficult it is to attain a flat response.
A block of five wax/paper capacitors is included to bypass the type 226
filaments (both sides) to the chassis,
bypass the 135V line to the chassis,
and bypass the ‘ground’ to the 135V
and -9V rails.
There are some unexpected connections in both this and the main filter
block in the power supply. I expect the
engineers were minimising the component count and making the best use
of the space available.
The three RF and first audio stage
valves (type 26) have a grid bias of
-9V. While it is easy today to generate
any DC voltage, in 1927, ingenuity
was required to keep the design simple. Cost and the availability of skilled
repair people required that these early
mass market sets were straightforward.
Power Supply
The AC is rectified with the UX280
valve, new for 1927. It was followed by
a choke input filter, with the inductors
in the 0V path, probably to minimise
flash-over to the frame and electrolysis of the wires. A resistive divider and
wax paper filter capacitors provide the
four supply voltages and the ‘cathode
bypass’ for the output.
The connections to the series dropping resistors in the power supply
were arranged so that the chassis is at
-9V with respect to the filaments of the
type 26 valves. Their grids connect to
the chassis through transformer primary windings and the volume control
to provide the required -9V grid bias.
The detector has zero bias, and
the output valve is self-biased with a
1690W cathode-bias resistor from the
tap on the balancing pot across the
UX171 filaments to the -9V rail.
The power supply, shown in Fig.2,
generates DC voltages of -9V, 45V, 135V
and around 170V for the output stage,
as well as 1.5V AC, 2.5V AC and 5V
AC for the filaments. These DC voltages are measured from the ‘ground’
tap on the resistor chain, not the chassis, which is at -9V.
Restoration
At around 17kg, the radio is heavy. It
was in good condition when I received
it, with no major rust visible, and the
cabinet had no major damage. The circuitry is in two parts: a power supply,
with the radio linked to it via a multicore cable and secured with metal
screws through the cabinet.
I was able to remove these sections
easily, separating them by undoing
the screws connecting the cable to a
tag strip on the radio.
I have worked on many transistor
and valve radios, but this was the dirtiest job so far. 100 years of dust and
fine dirt on the surface with wax and
pitch to be encountered later.
I first checked the mains transformer. If it was damaged, I felt it
would be best to preserve the radio
as-is. I replaced the mains cabling with
a three-core cotton-covered cable, with
a small fuse added in the Active line,
and the Earth connected to the chassis.
I applied 50V AC from a variac to the
mains input and left it for several hours.
The 220V/240V switch was set to 240.
I measured 62V a side for the HT, 1-2V
for the filaments and the transformer
The original waxed-paper capacitors
were all packed into a small metal
box. Not surprisingly, 100 years later,
they have become leaky.
did not heat up. It was left to run for
a while on 120V AC, then 240V AC.
I estimated the HT current requirement as being 15mA for the output
valve and 5mA for the others, giving
40mA in total. To emulate this, I connected an 18kW across the HT windings. With 230V AC at the input, the
outputs were 586V AC across the
whole HT winding (~293-0-293V AC
centre-tapped), 1.49V AC, 2.21V AC,
and 5.05V AC, and the transformer
stayed cool.
So, the mains transformer was functional, and the restoration could continue.
The two chokes (reactors) were next.
One measured around 11H, the other
0.6W, a likely short circuit as the insulation on the wires to it was crumbling.
They were encapsulated in pitch. Two
removal procedures are suggested:
warming with a heat gun, or dissolving with paint thinners.
I used paint thinner; the heat gun
approach would probably have been
less messy. With both inductors out,
The rear of the Radiola 17 with the back taken off. The power supply circuitry is contained in the enclosure on
the far left of the interior and its circuit is shown in Fig.2 opposite.
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March 2026 95
Table 1: replacement resistors
Original
resistance
Nominal New resistor
voltage
410W
135V
390W 5W
3750W
45V
3.9kW 5W
2140W
45V
2.2kW 5W
205W
-9V
200W 5W
1690W
30V
3.3kW 1W ||
3.3kW 1W
they looked alright, so I checked them
with a bridge. The second one measured 18H; my simple RLC transistor
checker gives up at 15H, so it read as
a resistor.
The wires were in poor condition
and heavily oxidised. I cut them near
the choke and cleaned them with
many passes over the ends with folded
emery paper. I then applied flux paste
and soldered new wiring to both, then
insulated the joints with heatshrink
tubing.
More of the original wiring was in
poor condition, so I replaced it with
segments from a length of HRSA seven-
conductor battery cable. The cabling
was laced to keep it tidy and preserve
some of the original appearance.
All filter capacitors showed significant leakage, so I replaced them. They
are housed in a large metal case and
held in with extra wax. It’s a beautiful
design that filters six different voltages
within a limited space. Unfortunately,
heating the wax did not release them,
so I had to cut a few out so the remainder could be extracted.
I replaced them with multiple 1μF
200V Mylar capacitors. As there is
plenty of room, I doubled the value of
each capacitor to provide additional
filtering.
The multi-tap wire-wound resistor
The volume control had degraded over
time and needed a delicate repair.
showed signs of overheating; most segments were open, and the rest intermittent. Ideally, new wire would be
wound on the ceramic former and
tapped, but I am not that skilled.
Using the voltages and other data
from the service notes, I calculated
the power for each segment. Assuming the original values would be accurate to within 10% at best, I selected a
combination of standard resistors, as
shown in Table 1.
The remaining working segments on
the original resistor were permanently
broken and new resistors placed under
the tags and connected to them. If a
future owner wishes to restore the original resistor, it is still there.
Seized tuning capacitor
The tuning capacitor would not
move. I oiled the shaft near the tuning wheel and left it for days. Eventually, it could be moved slightly, but it
was still very stiff. The tuning wheel
is made of pot metal (a brittle zincbased alloy), which was cracking, so
I had to treat it carefully.
The only way to free the movement was to remove the wheel. This
required knocking out the pin on the
shaft and, given the state of the wheel,
it may have disintegrated. I took measurements and photos so a new wheel
could be created if needed. Once the
pin was out, the tuning wheel slid off,
and the shaft rotated easily.
The pot metal had expanded and
was binding to the screw locating the
shaft. I filed the binding end to allow
the shaft to move sideways, to centre
the variable plates within the fixed
portion.
The wheel had to be stabilised, or
it would break in future. A local company suggested using epoxy glue, so
I purchased some E-143 metal epoxy
from Technicqll in Poland. I washed
the wheel to remove grease and oil,
then forced the glue into the cracks,
small sections at a time. I blocked the
shaft and tension screw holes with
Blu-Tack so I wouldn’t accidentally
get glue in them.
Once the wheel was repaired, I
refitted it with thin stainless washers
added to ease its movement where
the shaft was binding. I connected the
dial wire to the tuning shaft, stretched
it over the grooves in the wheel and
tightened it with the screw and clamp.
The radio had resistor/capacitor
coupling added between the first audio
valve and the output type 171, suggesting the coupling transformer was
broken. Resistance checks showed the
primary was open circuit. The transformers are located in a metal shell
clipped to the chassis, so I unsoldered
the wires from both transformers and
unclipped the transformer case.
It was filled with wax – better than
pitch, I suppose; I used a heat gun to
melt it. Both transformers are roughly
made, with no clamping of the laminations; they are ‘glued’ together
with wax. A suitable transformer
(very small, with a 3:1 turns ratio)
was donated by an HRSA collector.
I connected the wires from the failed
The tuning
capacitor wheel
had seized. Care
was required in
dismantling and
fixing it as it was
made of pot metal
that had become
brittle.
The series
wirewound
resistors (encased
in black, at top)
were bad so I
bypassed them
with a string of
modern resistors.
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transformer to it and refitted both in
the case.
Ideally, they would be installed
at right-angles to each other, but the
new unit was slightly larger, so I had
to make them parallel.
The antenna volume control was
another casualty of time; the resistive
element was corroded in places, and
the resistance wire had broken. Advice
from another HRSA member was to
bridge the broken sections by finding the ends, gently scraping off the
insulation with fine emery paper and
twisting them together. The resistive
wire does not solder, so the twisted
section was covered in conductive
silver paint.
There will be tiny (1-2 wire) sections
of the control that are missing, but for
its use as a volume control, it will not
matter. This repair worked perfectly.
The grid stopper resistors are wire
wound and tested alright. The grid
leak resistor is supposed to be 4MW but
measured as 3MW. I replaced it with a
3.9MW ½W resistor hidden under the
original red 4MW resistor.
The bypass capacitors are held in
metal cases clipped to the chassis. I
tagged and desoldered the connecting wires, then removed the assembly.
I then heated the cases and removed
the capacitors. The cases were washed
with vegetable oil (to dissolve the wax)
and detergent, glued together and the
capacitors replaced with 1μF and
2.2μF 250V polyester types.
I emission tested the valves and
replaced any that failed. With everything tested, I figured the radio should
work. The output transformer is a 1:1
type and the recommended anode load
for the UX171 (type 71) is 4.8kW at
180V. For initial testing, I used a 5kW
to 3.5W transformer and 4W speaker.
Fig.3: the frequency response of the set, either injecting a signal directly
into the detector output transformer (cyan) or directly to the antenna (red).
Expectations were lower in those days!
Having attached the multi-core
cable from the power supply to the
radio, I powered it slowly through a
variac with the UX280 out of circuit.
All valve heaters were operational.
Plugging in the rectifier gave the voltages shown in Table 2. All were a bit
high, so I needed to swap in a ‘worse’
type 80.
For further testing, I employed the
HRSA mini transmitter and a 1m wire
antenna. The signal was tuned in easily, and the volume control had to be
wound down to minimise distortion.
With no signal, there was some 100Hz
buzz from the medium-fidelity test
speaker. Examining the output with
an oscilloscope, there are noise spikes
of around 1V peak-to-peak at 100Hz.
Tracing back through the circuit,
they were present on the detector anode but not on the grid. The
+45V rail (and other voltages) had
some ripple, but no noise. I suspect
it is coupling between the two audio
transformers causing the problem.
50Hz hum was also visible, the minimum residual after adjusting the three
filament potentiometers.
I tested the receiver audio bandwidth but there is no specification for
this in the original documents. Removing the type 27 detector, I connected a
signal generator to the detector audio
coupling transformer through 10kW to
simulate the anode resistance.
Audio bandwidth is often specified
between -3dB points on the amplifier
response curve, but today’s amplifiers
have broad flat responses, and I feel
applying -3dB to this radio is not fair.
-10dB, or half the perceived loudness,
would be easily detectable but not prevent the signal from being heard. Here,
the -10dB bandwidth is around 4507500Hz (see the cyan curve in Fig.3).
The frequency response from the
antenna to the output is a similar
shape, with a more useful -10dB bandwidth of 200-4500Hz (the red curve in
The transformer between the audio preamp and
audio output stages had gone open-circuit.
Table 2: voltages on initial power-up
The tuning
capacitor wheel after
filling the cracks with glue.
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Australia's electronics magazine
Rail
Reading
Raw HT
175V
135V
151.3V
45V
52.8V
9V
9.1V
UX171 filament (5V)
5.1V
UX226 filament (1.5V)
1.5V
UY227 filament (2.5V)
2.2V
Bias on UX171 filament
(-30V)
-26.8V
March 2026 97
A better look at the chassis of the Radiola 17.
Fig.3). The RF bandwidth of the TRF
is generally much wider than a superheterodyne set, but in this set, it tapers
off from about 1kHz.
A possible cause is that there are no
trimmer capacitors on the tuning gang,
and it is quite likely the three sections
are not aligned, leading to unpredictable bandwidth of the tuned signal.
The lack of trimmer capacitors made
factory alignment critical and limited
user retuning.
The audio from a music CD played
over the mini transmitter was quite
intelligible on the bench test speaker
and not (to my tin ears) greatly distorted.
Cabinet restoration
The timber cabinet for this radio
is in very good condition for its age.
There are scratches and a probable
burn mark on the top, but the other surfaces are reasonably clear. It is missing
the hood over the dial light, a common
problem with these radios.
I considered refinishing the cabinet,
but it is 100 years old and you can’t
expect it to be in mint condition. So I
simply cleaned the timber and rubbed
it down many times inside and out
with a mixture of 50/50 white spirits and linseed oil. The appearance
remains consistent with its age.
Over time, the brass escutcheons
have oxidised and discoloured. I
washed them but didn’t polish them,
so that they and the cabinet look right
with each other.
RCA Speaker Model 100A
The RCA 100A speaker was sold
with this radio, and this one was
bought at an HRSA auction. The case
is made of pot metal and it is breaking
up in parts; small sections have flaked
off. I will clean it up and repaint it in
the future.
The speaker is a high-impedance
device, as were the horn speakers and
headphones of the time. When connected to a (late model) radio through
◀ Fig.4: the unusual
construction of the
RCA Model 100A
loudspeaker.
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Australia's electronics magazine
a step-up transformer, it works with no
grating or scratching noises.
It is a moving armature design
(sometimes called ‘balanced armature’). Fig.4, from the RCA Model 100A
Service Notes, shows the mechanism.
Not shown is the armature sitting close
to the pole pieces of a horseshoe magnet. Changes in the magnetism of the
armature from the coils will cause it
to move to one or other pole piece at
one end and move the drive pin at
the other.
The motor is small, at 40 × 25 ×
40mm, and sits within the magnet.
There is a low-pass π filter between
the input and the drive coils; possibly the speaker mechanism rattles if
driven with high-frequency signals,
so they are filtered out. At the low-
frequency end, the cone is very stiff,
which would limit the low-frequency
response.
I checked the speaker frequency
response with the PC-based AUDio
MEasurement System (AUDMES).
The RCA 100A
loudspeaker is
housed in this
early Art déco
style pot
metal and
fabric case.
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Table 3: model 100A speaker
Frequency
Input impedance
100Hz
4.36kW
525Hz
11.82kW
2730Hz
2.0kW
4700Hz
8.7kW
A good-quality line transformer was
connected between the PC to the
speaker for impedance matching and
to increase the drive voltage. The
-10dB response is around 200-3500Hz
– see Fig.5.
The speaker resistance is reflected
back to the output valve, so I thought it
would be interesting to see how close
it was to the desired 4.8kW load specified for the type 71 valve.
I estimated the speaker resistance
by connecting it to a signal generator through a variable resistance.
When the voltage across the speaker
equalled the drop across the resistor, the resistances would be equal,
and the variable resistor could be
measured. With the π filter and the
speaker coils, a complex impedance
was likely.
I took measurements from 100Hz
to 8kHz and recorded the highs and
lows in Table 3. The input impedance
drops below the desired 4.8kW over
the range of 2-3kHz, but generally it
is well above it.
Listening to a CD received from the
mini transmitter via the radio and RCA
speaker, it is not HiFi, but the music
was clear. I expect at the time it was
released, people would have been very
impressed.
Fig.5: the frequency response of the RCA Model 100A loudspeaker.
Screen 1: the repaired radio set picked up some mains hum and buzz. Partly
this could be due to its unshielded TRF construction, but my replacement
audio coupling transformer having to be reoriented might have also negatively
impacted its EMI rejection.
References
• Deeth Williams Wall: siliconchip.
au/link/ac7v
• RCA Victor Service Notes: 1923
to 1928
• RCA Service Data: 1923-1932
Vol. A
• RCA Loudspeaker Model 100A
Service Notes, June 1927
• Don Sutherland NZVRS Bulletin,
Vol 5 Number 2, August 1984
• RCA Radiola 17, Eric L. Santanen,
Bucknell University
• https://sourceforge.net/projects/
SC
audmes/
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A close-up of the loudspeaker moving armature motor.
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