This is only a preview of the March 2026 issue of Silicon Chip. You can view 34 of the 104 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Articles in this series:
Items relevant to "Solar Panel Protector":
Articles in this series:
Items relevant to "DCC Booster":
Items relevant to "Self-powered Wireless Switches":
Articles in this series:
Items relevant to "The Internet Radio, Part 2":
Items relevant to "Graphing Thermometer":
Purchase a printed copy of this issue for $14.00. |
SERVICEMAN’S LOG
Doing the dirty work
When a kitchen appliance fails,
among the most dreaded must be
the dishwasher. When it stops midcycle and refuses to proceed, you
can’t troubleshoot without first
removing the dirty dishes and bailing out
the greasy, soupy water in the sump. It is tedious
and unpleasant, to say the least.
The second, more physically demanding chore, is to
extract the beast from its cavity under the kitchen bench.
At some 50kg, our failed dishwasher is no lightweight, and
its German designers never thought to equip it with roller
wheels (for some reason).
Despite putting up stiff resistance, with a combination
of tugging while simultaneously rocking it side to side, it
gradually emerged, exposing 10 years’ worth of grime and
dust. Now at last I could remove the metal side panels and
get to the inner workings.
This unit had performed faultlessly for 10 years and had
always delivered great results. Its sudden and unexpected
failure suggested a problem that might be simple or obvious. At least that’s what I hoped. I decided to run a short
cycle to better observe its behaviour leading up to the point
where it would stop.
It began normally. The drain pump cleared the residual water, then it refilled and began the pre-wash cycle.
However, after a few minutes, it just stopped with the time
remaining indicator showing zero. It had failed to progress
to the main wash, which was baffling.
The water was getting to where it should be, the circulation motor was running and the water was pumping
out during the initial drain. All conditions necessary to
proceed seemed to have been satisfied, so why did it stop
prematurely?
84
Silicon Chip
I hoped that a Google search might help me locate some
service information or a schematic, but the corporate world
protects its secrets. However, I found an abundance of YouTube videos pointing toward the usual suspects being blockages, pump failures, or a failed heating element. These all
checked out OK on our machine.
The heating element is part of the main pump unit. Being
connected to the control unit by heavy-duty wiring makes it
easy to identify for the purpose of checking the resistance.
This was as it should be, at around 20W.
Having eliminated the prime suspects, the remaining possibilities seemed to be that the control module
itself may have failed, or perhaps a malfunctioning sensor could have confused the control module, leading
to a shutdown. I removed the control module for close
inspection, but it looked pristine with no components
damaged or burnt.
From past experience, I knew that a sensor that failed
to return the expected signal could cause a dishwasher
to stop mid-cycle. Years ago, many dishwashers (and
washing machines for that matter) had a motor-driven
switching mechanism. The motor advanced the mechanism, and a large knob on the front of the dishwasher
rotated accordingly to indicate the progress through the
program.
I had a dishwasher like that; it had both cold and a hot
tap connections. The main wash cycle used only hot water.
When the hot water solenoid went open-circuit, the motorised switch would be paused, waiting for a signal from
the water level sensor. With a failed solenoid, the required
water level would not be reached and, in the absence of a
signal, the motor would not be powered on.
At that point, the program would be abruptly halted.
The result was not unlike what I was experiencing with
the current unit.
Motorised switches have long been replaced with microprocessor electronics, enabling more advanced functions,
including the reporting of error codes. Unfortunately, I
had no error codes for guidance and no service information that might have given a clue about how many sensors
there were or what functions they performed.
Australia's electronics magazine
siliconchip.com.au
I was on the verge of giving up. Judging by the wiring
that snaked throughout the machine, most of the sensors
appeared to be well buried in the bowels of the device.
However, there was one sensor that stood out.
Most of the space on one side of the dishwasher is taken
up with a large, translucent plastic box containing an intricate labyrinth of water galleries. I’m guessing that its purpose is to store and regulate the inflow of water, and it may
also save energy by warming the stored water using heat
released during the wash cycle.
Mounted in a recess on the plastic box is one very obvious sensor that is easily accessible, shown in the accompanying photo. I decided it was worthy of closer examination as a last resort.
It appears to be a flow meter, which lives in the water
inlet path. A small, bladed impeller with an embedded magnet rotates with the flow of incoming water. With a torch,
I could faintly see it spin inside its translucent housing.
Sitting outside in a recess was a reed switch, a glass capsule with metallic contacts that should close each time the
impeller magnet passes.
I can only speculate about the purpose of this sensor. It is
obviously able to inform the controller about the flow rate
and volume of water entering. Maybe it’s a safety device.
Perhaps a runaway count might signal an overflow of water,
prompting a shutdown.
Alternatively, if the impeller seized or the reed switch
failed to register, the controller might be programmed to
halt the process due to failure of the device for safety reasons or because insufficient water had been received.
The reed switch was mounted on a small circuit board
and was easily removed for testing using a simple magnet
and multimeter. The contacts inside the glass envelope
would close as they should when the magnet came near. I
could not fault it, but decided to reinstall it anyway.
I ran the short cycle again. This time, the cycle progressed
properly, and the machine ran for the full duration of the
main wash but then stopped, showing an E14 error code
for the first time. It had failed to perform the final, critical
drain. It wasn’t a complete cure, but it was pleasing progress nevertheless.
siliconchip.com.au
A quick consultation with the internet confirmed that E14
was indeed associated with a flow meter fault or a problem
with the water intake. Could it be that the reed switch had
aged and become unreliable?
I have had some previous experience with reed switch
faults. In the 1980s, new telephone exchange equipment
was installed that employed reed switches. Error reports
showed that some reeds mounted on circuit cards were
prone to sticking. To prove the fault, the cards needed to
be very gently removed and the suspect reeds checked
with a multimeter.
Sure enough, certain reeds on the board were sticking
with contacts closed. The gentlest tap on the card was
enough to cause the contacts to open with an audible click.
A quick trip to Jaycar and I obtained a visually identical reed switch for less than the cost of a cup of coffee. I
soldered the new one in place of the old one on its circuit
board and reinstalled it. I pressed Start.
Success! The dishwasher ran perfectly, advancing
through every stage, including the final drain. Incredibly,
an expensive dishwasher had been brought to its knees by
quite possibly the cheapest component in the entire device.
Alan Preacher, Briar Hill, Vic.
The red arrow points to the recessed sensor located in a
plastic housing. This sensor is likely a flow meter.
Australia's electronics magazine
March 2026 85
Dredge boat radio repair
In the distant past, I was married to a Sydney girl, but
we lived in Newcastle. One weekend, we were visiting the
relos in Sydney when the brother-in-law, an electrician,
stated he was on call for the port of Botany Bay for the
weekend, and had a call out for the dredge that had twoway radio problems.
He said, you know more about electronics than I do; can
you come with me?
We went to the dock, and a tug was waiting to take us
to the dredge. When onboard and taken to the radio room,
we found that the radio was relaying all calls received and
making an echo on the network.
I picked up the mic and asked the harbour master for a
radio check. He told me that the problem was still there.
I then realised that I had not heard the clunk of the relay
switching to transmit mode. We opened the box (about half
a meter square) and found the relay. It was plugged into
the circuit board.
The points were fused together. We managed to separate
them with a screwdriver. We found the onboard chippy and
got some sandpaper from him to smooth them out. That
got it working again, for the time being. We also asked the
chippy to tell the electrician, on return from his break, to
order a new relay.
They fed us dinner and gave us some beer. As my brother-
in-law was on call, he was not allowed to drink, but I was,
so that was my pay for doing the job! We had to wait about
two hours for the tug to come back.
Mick Toomey, Newcastle, NSW.
Breville microwave repair
My wife told me that there was something wrong with
our microwave, as it sounded different from usual. I could
tell from how it sounded that the cooling fan had stopped
working. I was hoping that it was just the fan motor, as
that would be an easy fix as long as I could find a replacement part.
We found this microwave at one of the local tip shops
about four years ago. It was in almost-new condition but
needed a good clean as it had obviously been stored for
an extended period. Until now, it had been very reliable.
I took the microwave to my workshop and removed the
six screws that hold the cover on. The fan is located in
the back right-hand corner. I disconnected the two wires
going to it and got out my multimeter to check the resistance of the winding. The winding was open-circuit, so
that explained why the fan no longer worked.
The next question was whether I could find a replacement fan motor. I started by unscrewing the circuit board
on top of the fan housing, then I removed the screw from
the back of the microwave that was holding the fan motor
housing in place. To remove the fan motor housing from
the microwave, I had to first remove the magnetron, as it
was stopping the fan motor housing from tilting forward
enough to remove it.
An eBay search for a fan motor to suit this model of the
microwave was not successful, although I did see one or
two listings. I changed my search to the part number of
the motor, and I found a couple more listings from China,
but when I switched from default to Australia only, there
were none.
I changed my search to worldwide and set the search to
price plus postage, lowest first. This showed many listings
for this part, and it also showed that this exact fan motor is
used in a multitude of different brand microwaves. I was
able to purchase a replacement fan motor for $15.27 with
free postage, but I would now have to wait for it to arrive
from China, which could take up to four weeks.
In the meantime, my wife found another microwave at
the local tip shop for $10 and it was still in very good condition. It had been tested before she purchased it to make
sure that it worked.
Amazingly, the new fan motor arrived in just 11 days
from China. It was obviously an after-market replacement,
as it did not have the part number on the side like the
original motor. The next problem was that I was unable
to remove the fan from the old motor. However, I was able
to change the rotor, with the fan blade attached to it, into
the new stator.
The two motors were almost exactly identical, enabling
me to swap the parts, and the rebuilt motor worked as
expected. I reassembled the microwave and tested it by
putting a cup of water in it and running it. I could hear
that the fan was running, and the microwave sounded the
same as it did before the fan failed.
Good-sized new microwaves cost around $150-300,
so being able to repair this one for less than $20 was
well worthwhile. The spare microwave for just $10 was
a bonus.
The interior of the Breville microwave (left), fan motor
(above) and the repaired device (right).
86
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
WARNING: Microwave ovens contain very high voltages that are extremely dangerous. A microwave can retain
these high voltages even after it has been turned off and
unplugged, and even a dead microwave can kill you, as
this high voltage may not dissipate for a long time in some
circumstances. So if you are not experienced in repairing
microwave ovens, do not remove the cover.
Bruce Pierson, Dundathu, Qld.
Turntable inverter repair
This story has a lesson about buying semiconductors from
online vendors. I recently built the turntable inverter from
the May 2016 issue (siliconchip.au/Article/9930). Everything went well with the assembly, and I decided to benchtest it before fitting it into its diecast box. This meant that
the Mosfets were not yet heatsinked.
I connected a 12V car test lamp, drawing approximately
180mA at 12V, across the transformer terminals on the circuit board, with an oscilloscope probe connected as well. I
connected a linear power supply set at 14V DC. To my disappointment, the test lamp flickered randomly, and within
about 10 seconds, there was a burning smell.
I quickly switched it off and found that the IRF9540
Mosfets were stinking hot. Surprisingly, the IRF540 Mosfets were at about room temperature.
Troubleshooting was going to be difficult as I had to connect scope probes to the circuit, switch it on, quickly make
measurements, then switch off. I tried tracing waveforms
using this tedious procedure. It was getting ridiculous, so
I removed IC3 from its socket, then bent pins 1 and 7 horizontally so they would be disconnected when I plugged
IC3 back in.
I was now able to trace all the waveforms up to the inputs
of IC3. They were all correct 50Hz sinewaves (I had set the
inverter to 50Hz mode). The output pins of IC3 (1 and 7)
were putting out square waves, but they were not driving
the transistor section, so I desoldered all four Mosfets, bent
the pins of IC3 back to their original positions and powered it up again.
I could detect sinewaves at the bases of Q5, Q6, Q7 and
Q8. I powered it down and performed continuity checks
to verify that each component in the circuit was connected
correctly. I couldn’t find any faults; all components tested
OK and were in the correct places.
To make troubleshooting easier, I soldered header sockets
siliconchip.com.au
Items Covered This Month
• A prematurely stopping dishwasher
• Dredging up a boat radio
• Breville microwave repair
• Finding the culprit in a turntable inverter
• Following the breadcrumb trail
• Repairing a NAD 701 stereo receiver
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that your
material must be original. Send your contribution by email to:
editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
in the Mosfet positions so I could easily swap them over. I
put in all new Mosfets and powered it up. The same fault
appeared; the Mosfets got hot again quickly.
I then tried bypassing IC3 by removing it from its socket
and using tinned copper wire. I bridged IC3b pins 5 to 7
and IC3a pins 3 to 1. This produced a square wave at the
transformer terminals, and the Mosfets ran cool.
I suspected that IC3 could be faulty and replaced it with
the one spare I had on hand, with no improvement. As the
pinout of IC3 is the same as an LM358, I tried that again
with no success.
I then noticed that the output waveform to the transformer terminals was a half sinewave, but it had oscillations superimposed on it at about 15kHz.
If I powered the circuit off and then on again, the circuit would start up without oscillations, and the Mosfets
would run cool with a clean sinewave at the transformer
terminals. As soon as I put a scope probe on the output or
anywhere in the circuit, the oscillations would start and
the Mosfets would again overheat.
Everything checked out up to IC3, the Mosfets had been
replaced and I could find no faults in the driver circuit, so
I purchased a couple of LMC6482AIN op amps from Jaycar (to replace IC3) and that was it. The inverter sprang to
life, and I could not get it to oscillate anymore.
I have purchased lots of components online over the
years and had good luck with only one dodgy purchase
(previous to this one) in that time.
I have noticed that there are a lot of YouTube videos
online regarding testing for dud op amps, Mosfets etc.
Online bargains could be duds, so you should put the
device through its paces and ensure that the test results
agree with the device datasheet specifications before installing it. This is time-consuming but can save you a lot of
work and time later.
Australia's electronics magazine
March 2026 87
In spite of all the frustration, I did learn a lot about this
circuit, and it was very satisfying to be able to finally nail
the culprit.
Geoff Coppa, Toormina, NSW.
Russell Hobbs toaster repair
We have had a Russell Hobbs four-slice toaster for some
years. While a little bulky for the benchtop, its saving grace
is its capacity to toast all four slices evenly on both sides at
the same time. Previous toasters had achieved only various
patterns of brown and tan, sometimes black, so when the
Russell Hobbs ceased to function, it was a sad day indeed.
While one side of the toaster still functioned, the other,
much more frequently used side (the one closest to reach!)
refused to light up. It had started to work erratically a few
days leading up to the final failure. There is a history in
the house of repairing white goods and appliances instead
of replacing them, so the toaster duly made its way to the
workbench.
Taking the top cover off, the workbench and the technician was quickly covered in crumbs – quite an amazing
amount, really. The internals of the plastic chassis included
the toasting chamber with the heater elements and components of the two bread carriages, including springs and
bread racks.
In front of the chamber, a set of contacts for each of the
carriages is connected to the mains supply. These close
when the bread carriage lever is depressed. Beside the
contacts, a release solenoid, visible at the top of the photo
(shown below), holds the carriage down when energised
until the desired level of toastiness has been achieved, then
releases the carriage.
On each side of the chamber, a small circuit board
receives mains from the carriage contacts. It has various
components, including an DPST relay that energises the
carriage solenoid. This board also supplies 12V DC to, and
is controlled by, a timing circuit board mounted in the top
cover. The timing board has various functions, such as
defrost and warming, and energises the relay.
At the top centre of this photo, you can see just a bit of the
release solenoid, while below it is the 12V DC DPST relay.
88
Silicon Chip
Once all the breadcrumbs were cleaned up, the diagnosis of the fault was quick. On the side that wasn’t working, the DPST relay had lost a large portion of its plastic
cover due to contact arcing, judging by the look of the
relay contacts. As with most appliances these days, they
are not made to be repaired, and extracting the circuit
board without breaking all the plastic fastening tabs was
a mission in itself.
Once removed, further examination revealed that the
board had got rather hot underneath the bridge rectifier,
which was mounted flush on the board. The rectifier failed
testing and was replaced but elevated off the board. The
electrolytic cap also tested bad and was replaced. All other
components tested OK.
The DPST relay was not so easy to replace due to its size
and pin layout. A replacement was found from one of the
major component suppliers, but with a rather eye-watering
cost once postage was included. The parts cost less than a
new toaster, but not by much!
After testing the other circuit board, replacing the bridge
rectifier and capacitor, two replacement relays were ordered
– might as well replace both. Delivery was prompt, and the
new relays were installed. The opportunity to check the
mechanical operation of the toaster was also taken, cleaning
the carriage contacts, straightening some bent components
of the bread carriage, and general de-crumbing.
After reassembly and testing, both sides were found to
be working correctly. All up, the time to repair the toaster
was around two hours. Still, there is the satisfaction of
keeping an appliance in service and not going into the
hard waste collection.
Richard Dilena, Ocean Grove, Vic.
NAD 701 stereo receiver repair
The ad stated, “NAD 701 parts only untested with the
display not working”. For $50, it had to be worth a try. In
the worst case, replacement displays are available, and
swapping them can’t be that hard.
So I bought it, opened up the case and looked at the
display PCB. The display is backlit, and one of the incandescent lights had failed. The power to the lamp was 12V
DC, so I replaced the 4.7W current-limiting resistor with
a 560W value and inserted a high-intensity green LED in
place of the incandescents (see the photo opposite). That
got the display working.
The power amplifier voltages are regulated (along with
most supply rails in this amplifier) and they were all
within tolerance. I checked out the amplifier by playing
a CD, and the amplifier was working with no apparent
distortion. I also tested the phono preamp, which was
also functional.
Next, I tested the tuner. It is built around three ICs and
an FM tuner front-end from Mitsui. I could change the
AM & FM tuning frequency on the display, but there was
no change in the sound. It was like the oscillator was not
working. In this receiver, AM and FM are tuned with varactor diodes powered from an LM7000 IC through a Darlington transistor pair amplifier.
The LM7000 has an onboard oscillator with an external
7.2MHz crystal followed by a frequency divider of 145 times
for AM and 1007 times for FM. There is a second divider
programmed from the display output that is fed by the AM
or FM voltage-controlled oscillator (VCO).
Australia's electronics magazine
siliconchip.com.au
Shown above is the circuit diagram for the tuner and the replacement I made for the backlight, using a high-intensity
green LED and 560W series resistor. Below is the front panel of the NAD 701 stereo receiver and a close-up of the tuner
section of the board showing some of the adjustment points.
The frequency and phase difference between the two
divider outputs is compared and converted to a voltage
proportional to the phase and frequency difference. The
amplified voltage determines the VCO frequency; as the
comparator ramps the voltage up (or down), the AM (or
FM) oscillator frequency changes until they match.
Test point 1 (TP1) is the voltage applied to the VCO (AM
or FM) and it was stuck at 40V. Pin 17 of the IC (charge
pump output) was also fixed, so the transistors were likely
alright. An oscilloscope on pin 20 of the IC showed no
oscillator output. Adjusting the small variable capacitor
in the crystal circuitry made no difference, so I replaced
the LM7000.
Once the decision to remove an IC is made, avoiding
siliconchip.com.au
damage to the PCB is the highest priority. So I cut every leg
of the IC near the chip and desoldered them individually.
I then soldered a socket in place and inserted a replacement IC. Adjusting the trimmer capacitor brought the circuit into oscillation.
The AM tuner then worked well, but there was no
change in the FM behaviour. The supply to the FM frontend module is 12V through an inductor/capacitor RF filter.
There was 12V on the supply side of the 2.2μH inductor
but not the tuner side. Replacing it brought the FM tuner
to life as well.
The story could have ended very differently, but in this
case, it was $50 well spent.
SC
Jim Greig, Mount Helen, Vic.
Australia's electronics magazine
March 2026 89
|