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SERVICEMAN’S LOG
Closed for Christmas!
Dave’s on an early holiday, so this
month we’re instead featuring some of
our contributor’s items, starting with
a weather station that was fixed up
by Bryce Templeton. Despite
being a solar-powered unit, it
still needed non-rechargeable
lithium cells.
I bought a new weather station about three
years ago to replace an old one that had
fallen to bits. I purchased it online as, at the
time, store-bought units did not offer what
I thought was a handy option: solar cells to
power the outdoor section. That would save
me having to pull the unit down to change batteries.
I should have done more homework, as when it arrived,
I found that it still required batteries and I was warned in
the instructions not to use rechargeable cells. In fact, they
recommended using non-rechargeable lithium cells. I didn’t
have any lithium cells on hand and, as I was keen to get it
going, I used ordinary alkaline AA cells, which worked fine.
The theory of the solar cells was that the unit will run on
solar if it is available; otherwise, it is powered by the batteries. This results in the batteries needing to be changed
about every six months.
This was the situation for more than a year, when I noticed
that a section of the indoor display was blank. This was the
section that shows the intensity of the sunlight in W/m2,
and the UV index. So the next time I had to change batteries, I decided to investigate this problem.
An examination of the device showed that while it was
well made mechanically, electronically, it was a different
story. Getting it to connect to the home WiFi had been an
arduous task, and it never managed to send anything to
Weathercloud.
Items Covered This Month
• Fiddling with a finicky solar weather station
• Bruce Pierson’s troubles: lights, fans and angle
grinders
• Repairing a foldback monitor speaker
• The bargain bin 65-inch TV
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
86
Silicon Chip
Anyway, I took the covers off and discovered that the
sunlight sensor is a tiny disc-shaped PCB containing an
unmarked IC encased in clear material. It lives in a tower
with a small window on the top of the unit. Examination
didn’t show anything unusual, so I did a quick re-solder
of the ribbon cable that connects to the main board, which
of course did nothing.
Alongside the sunlight sensor is a bubble level, apparently so that the unit can be mounted truly level, which is
important for tipping-bucket rain gauges. Unfortunately,
in most installations it can only be seen from a helicopter or drone.
I decided to try to get a replacement sunlight sensor and
sent off an email to the firm I had purchased it from. After
several very confusing emails, in which they never said if
they actually sold parts or if they had this part, they came
up with the best ‘catch-22’ I have heard: even if they did
have the part, I would not be able to buy it from them unless
I had previously bought one.
At this point, I gave up on the sunlight sensor. However,
on this battery change, I decided to try the lithium cells
they recommended. It seems that alkaline cells have problems if the temperature drops below zero, whereas lithium
cells will operate to -20°C. There is not much chance of
even 0°C here, but I thought they might last longer, so at
great expense, I purchased a pack of four. I installed three
of these, and all was well.
I was very surprised about a week later to find the outdoor unit not transmitting. Down it came again, and I found
the 4.5V battery reduced to about 1.5V. Measuring each cell
revealed that one cell was reading about 0.5V in reverse!
I decided that I must have gotten a dud cell and replaced
it with the remaining new cell, and we were away again.
Australia's electronics magazine
siliconchip.com.au
The weather station, both mounted and lying around (shown left), and the output data provided on the internal display.
But not for long; a week later, again no transmission.
Again, down came the unit, and again, I found one cell with
reversed voltage. Closer investigation this time revealed
that with no batteries inserted, there was about 2V at the
battery terminals. The penny dropped; I took the unit out
into the sun, and the voltage at the empty battery terminals shot up to about 7V!
After tracing the circuit as best I could, I came to the
conclusion that the solar was an add-on, as there was no
circuitry on the main PCB to do with it. It seems that the
solar cells are just paralleled with the battery, using the
battery as a voltage regulator to prevent the voltage from
going too high in strong sunlight.
Apparently, alkaline cells tolerate this treatment, but lithium cells strongly rebel. This would indicate that although
the instruction book recommends lithium, it had never
been tried in practice, or more likely, the book was written before the solar addition came about.
The solution? Well, it’s currently running with no problems on alkaline cells. A proper solution would be to use
some sort of charge regulator and fit rechargeable cells.
Editor’s note: maybe this is a case of confusion between
lithium and lithium-ion cells, as noted in my July 2025
editorial? Still, charging lithium-ion cells without current
or voltage limiting is a bad idea!
Bryce Templeton, Mudgeeraba, Qld.
Bruce Pierson’s troubles around the globe
My wife asked me to replace a light globe as it was not
working. I checked our box of spare globes, but I did not
have that wattage, only the next wattage up.
I decided to use a globe from the lounge room to replace
the failed globe and put the higher wattage globe in the
lounge room. But when I put the new globe in the lounge
room light, it did not work. It was brand new, so I was not
impressed.
On inspection, I could immediately see why it didn’t
work. One of the contacts on the base was completely
missing. I wondered if I could repair it by using a contact
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from the failed globe. I managed to prise out the contact from the failed globe with the point of a knife, so it
looked possible.
I tried to push the contact into the hole in the base of
the new globe, but it kept popping out. I could see that
there was a springy wire in the hole that was causing
this. It seemed that the wire should be on the side of the
hole and not in the middle, so it was a manufacturing
fault. This also explained why the original contact had
come out.
I managed to bend the wire into the correct position
using a small flat-bladed screwdriver, and that enabled me
to push the contact in and it remained in place very firmly.
I put the globe into the light and it worked. Of course, I
could have taken it back for a replacement, but I presume
it would have ended up in landfill despite such a simple
fault. That would have taken up more of my time, too.
This was an unusual situation that I have not encountered previously. It must have been missed in the quality
check, or maybe the contact fell out during transporting.
It’s always pleasing to rescue these devices.
A wall-mounted fan repair
Our son had been using a Heller wall-mounted fan. My
wife asked me if I could clean it and put it away, as our son
no longer needed it. I asked her if it still worked, and she
told me he’d said that it worked the last time he used it.
I started by unclipping the front guard and removing
it. Then I unscrewed the blade retaining nut, which is a
left-hand thread. That enabled me to remove the blade for
cleaning. Then I thought I had better test the fan before
cleaning to ensure it did work. There was no use in cleaning it if it didn’t work.
This is an electronically controlled fan, and sometimes
such types decide to stop working for some reason. In this
case, when I pressed the start button, nothing happened.
I felt the blade spindle, and I could tell that the motor
was trying to turn it, but it was not succeeding. This indicated that the bushes had run dry and seized, which is a
Australia's electronics magazine
February 2026 87
cosmetic condition, but they are a lot more reliable and
longer-lasting than newly purchased fans, which often fail
when they are just out of warranty.
A bit of work, some lubrication and a good clean, restored
this fan to good working order again. The photo opposite
shows the fan after repair and cleaning.
Following with a Bosch 9-inch angle grinder
common thing to happen with fans, so I switched it off
and unplugged it.
I then refitted the blade so I could turn the fan, finding
that it was very difficult to turn. I removed the blade again,
then unscrewed the nut holding on the back guard and took
the fan out to my workshop.
With a #2 Phillips screwdriver, I removed the four screws
holding on the front plate that the back guard is attached
to, then I removed the rubber plug on the back of the motor
guard and unscrewed the single screw and removed the
motor guard. I refitted the blade so the fan could be turned
over by hand.
Next, I put a few drops of engine oil on the front bush and
turned the fan multiple times. It was still difficult to turn,
so I added a few drops of engine oil on the back bush and
continued turning the fan by hand. Repeating this process
several times eventually freed up the bushes, and the rotor
spun freely, so I removed the fan blade again.
After wiping up the excess oil, I plugged the fan in to test
it, and it worked nicely, so I refitted the back motor guard
and the front plate after cleaning them. It is better to use
engine oil when servicing fans, rather than machine oil,
which is too light for this purpose. I have used this process many times on various fans (including exhaust fans)
with good results.
With the fan working again, I finished the cleaning job.
I used a brush to clean the front and back guards, then
a damp cloth to wipe the blade clean. I dried it with a
dry cloth. This blade cleaned up easily, as the fan was
relatively new. I reassembled the fan and gave it a good
test run on all three speeds.
As it was now working correctly, I put a cover on it
and put it away for future use. This particular fan has a
bracket that is screwed to the wall, and the fan sits on
that bracket, so it isn’t really portable.
When cleaning fan blades, I’ve found in some cases that
it is sometimes necessary to use a brush and soapy water if
the dirt is really stuck to the blade; still, they mostly come
clean with a damp cloth.
The hardest fans to clean are used fans we pick up at
the Tip Shop. These old fans are usually not in very good
88
Silicon Chip
I can’t remember where I got this 9in Bosch angle grinder,
but I’ve never used it. I’m used to 100mm and 125mm
angle grinders; this one is much scarier at 230mm. Still,
I needed to cut some concrete, and the smaller grinders
just would not cut deeply enough. I managed to find a
230mm diamond blade on eBay for $27.20 (they are normally over $100!).
The grinder did not come with a tool for replacing the
blade. I found the correct tool on eBay, but it was $30,
so I decided to make one. I got a section of power pole
bracing that I’d picked up at the tip shop and cut it to
length. I then drilled three holes in it, and I welded a pin
in the two smaller holes. It was good enough to remove
the grinding disc that came on the tool and fit the diamond disc. I also fitted the side handle to the grinder
for added safety.
The grinder would not start if the disc was in the vertical position, but it would start with it horizontal and kept
running when turned vertical. After cutting the concrete,
I checked the cable and brushes; they were all good.
Later, when I needed to do some more concrete cutting, the grinder no longer worked. I removed the cover
and checked the switch with my multimeter. The switch
was open circuit with the trigger held in, so I would have
to replace it. I suspect that the switch had just worn out.
I found a switch listed for this model, but it was over
$30. It was a little different from the original but looked
like it should fit. I then changed my search criteria and
found the same switch listed for a slightly different model
grinder for $17.50.
Having eventually received it, I compared it with the
old switch. There were some differences, but the new
switch looked like it
should fit in the
case the same
way as the old
Australia's electronics magazine
siliconchip.com.au
The repaired fan (left) and Bosch angle grinder (right).
one. The main differences were the shape of the trigger
and the X2 capacitor being in a different place.
It fit nicely into the handle section of the grinder, which
comes off the main body after removing four screws. However, when I tried to plug the internal plug on the main
part of the grinder into the switch, it would not go over
the pins. I then realised that the pins on the end of the
switch were closer together on the new switch than on
the old switch.
I’m not sure if this was because the new switch was for
a later version of the grinder, or because I had ordered a
switch for a slightly different model. In any case, after
making some modifications to the plug and the switch,
they went together. Thankfully, the only real difference
was the size of the blank section in the middle of the plug
that spaced the terminals apart, so it was easy to modify.
I cut out the middle spacing section with a utility knife,
which left me with two separate insulated plugs. On my
first attempt, I found that I could not get the plugs onto
the pins, as the switch had a ridge in the middle of where
the plugs plug in, which the original switch did not have.
I used a utility knife to remove this ridge, then it all went
together.
It was quite a nightmare getting the grinder back together
because of the way the two handle halves went over the
switch and over the main body of the grinder. It took a lot
of trial and error to get everything lined up, and the two
handle sections correctly positioned on the main body of
the grinder. Then it was just a matter of installing the four
screws and the repair was complete.
A quick search revealed that it would cost $450-500 to
buy a new grinder like this. Because I got it for free and only
spent $17.20 for a new switch and a bit of time, I ended
up with a good quality Bosch angle grinder for a fraction
of the cost of a new one. I will repair anything that I can
get parts for!
Bruce Pierson, Dundathu, Qld.
Repairing a “VoiceSolo” foldback monitor speaker
The TC Helicon VoiceSolo foldback monitor is a self-
powered speaker designed to be used with a microphone
stand, with the mic boom attached to the top of the monitor. I was recently presented with one of a set of four that
was described as “dead” by the users.
siliconchip.com.au
Australia's electronics magazine
February 2026 89
The VoiceSolo preamplifier (left) and power supply (right), with the failed electrolytic capacitors circled in red.
The monitor case is of diecast aluminium, with the
front assembly containing the speaker and input controls,
secured to the main enclosure by four screws. Applying
power to the monitor and connecting an input signal confirmed no power indicator LED and no sound.
Opening up the monitor revealed a loudspeaker and four
circuit boards, one attached to the front assembly and three
within the rear enclosure. The power amplifier is a ‘BASH’
amplifier design where a Class-AB bridge amplifier module
is supplied with a main DC supply that is modulated by a
secondary switch-mode variable voltage supply tracking
the amplifier audio input.
This particular design has a 200W power supply and
amplifier module built on two boards by Indigo Canada.
A check with a multimeter at the main switch-mode
supply PCB confirmed a steady +60V DC main supply, but
none of the four low voltage rails, ±24V and ±15V, were
present. Visual inspection revealed a ¼W resistor burned
to a crisp and a 100μF 25V electrolytic ruptured.
This power supply derives its low-voltage rails from
an additional secondary winding on the main switching
transformer. A group of diodes and electrolytic capacitors
create unregulated positive and negative DC rails, which
are then fed through a 7824 linear regulator and a discrete
transistor regulator circuit to deliver ±24V rails for the
BASH amplifier control circuits.
A pair of 7815/7915 linear regulators supply the mixer/
preamplifier circuits. The ¼W resistor is connected between
the bottom of the secondary winding and GND, acting as
a fuse. A circuit diagram could not be found with extensive internet searches, so I needed a working monitor for
reference.
This duly arrived after a week, revealing the resistor to
be 100W. I replaced the two failed parts and reassembled
the monitor, unsure whether the fix would work.
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
90
Silicon Chip
I couldn’t spot any other components visually damaged;
I needed to test the low voltage rails before doing anything
more. Reconnecting the loom and powering on the speaker,
I was greeted with a green power light on the front panel,
so I grabbed the multimeter to check the rails. But before I
could take any readings, the resistor began emitting magic
smoke and failed again.
So, we have a burned-out resistor and a ruptured capacitor on the output of the 7915 regulator. What was causing this?
My best guess was a failed 7915 regulator, as it was feeding the failed electrolytic. Since it is secured to the heatsink with a shared mount to the other three regulators and
a TIP30C power transistor that delivered the -24V rail, I
decided to test the lot.
I removed the four from the circuit board and tested
the regulators on a breadboard. All were good, including
the 7915. So I reassembled the power supply board and
replaced the resistor again.
This time, I was wiser and powered up the switch-mode
supply board on its own on the bench. This time, the resistor didn’t fail, and all four low-voltage rails were within
spec. So the root cause was elsewhere.
The preamplifier, mixer and tone control board were
mounted to the front panel in an assembly comprising the
combined vent/carry handle. Dismantling the assembly
revealed a board with eight NE5532 op amps, 13 electrolytic capacitors and a mix of SMD components.
I was about to begin meter checking each of the NE5532
op amps when I noticed a very slightly bulging electrolytic
hiding among a cluster of four identical ones.
A closer look revealed that this was another 100μF
25V capacitor. In fact, all the electrolytics on the board
were 100μF 25V, of the
same make and type. I
removed the bulging
one and tested it on
the component tester.
Its value had risen to
over 150μF, and it had
a high ESR reading as
well.
The VoiceSolo
speaker and
I/O box.
Australia's electronics magazine
siliconchip.com.au
Given that the four DC regulator circuits were working
correctly, I began to suspect the electrolytic capacitors
themselves.
In for a penny, in for a pound, and out with the vacuum desoldering gun. I removed and tested all 13 of the
capacitors. Only five tested good! Some of the capacitors were functioning as supply bypasses, while others were for audio coupling. I decided to replace all the
100μF capacitors in the monitor with good-quality low-
leakage types.
For the ‘acid test’, I reconnected the wiring harness
and gingerly reached for the power switch. On powerup, it was a bit anti-climatic. No magic smoke, all supply rails within spec, green power LED on, good to go!
I reassembled the monitor and gave it a thorough bench
test, playing Sting at a modestly loud level.
With so many failed capacitors, I began to wonder if
this might be a manufacturing problem. Would it happen
again soon with the other three monitors? I checked the
spare that was used to identify the 100W resistor. In this
one, the resistor hadn’t failed, but sure enough, there were
another eight faulty electrolytics.
In the end, I dismantled and replaced the capacitors in
all four of these monitors. Testing revealed the majority in
each to be on their way out, with strange capacitance and
high ESR readings. In all, I replaced 60 capacitors.
Ray Ellison, Dover Gardens, SA.
The $19.00 65-inch television set
Dave Thompson’s article in the August 2025 issue
about repairing discarded devices struck a chord with me
(siliconchip.au/Article/18644). Over the years, while walking around the streets of McCrae, I’ve rescued many perfectly good items discarded by their owners and left on the
nature strip for council collection.
The list includes a Jensen X-125 subwoofer, a 150mm
reflector astronomical telescope, sundry computers and
laptops, to name just a few. However, my most rewarding
nature strip pickup was a large-screen Sony TV. It was buried under a pile of old plastic chairs, a mattress and other
paraphernalia, and barely recognisable as a TV.
I ventured onto the premises and asked the owner if
it was a TV, and why he was throwing it out. He said it
had simply stopped working, and as an expert IT consultant, he had concluded that “it was a transformer failure”
and not worth repairing. I was welcome to take it since it
would reduce the volume of his discards, and hence his
fee to the council.
siliconchip.com.au
The set was a 65-inch Sony Bravia KD-65X7000E of
about 2018 vintage. It was awkward to load into the car –
the thing was simply enormous and quite heavy – but we
made it home and successfully unloaded the device into
the shack for further inspection.
Fearful of flexing the set too much, I cautiously removed
its rear cover to be confronted by three PCBs: an RF board,
a motherboard and a power supply assembly. They were
absolutely dwarfed by the screen itself, and I wondered
how such a small set of electronics could drive such a
monster screen.
A quick check revealed that the power supply was not
working, further confirmed by two blackened diodes, which
had obviously ‘released their smoke’. Without really checking these diodes, I reckoned a couple of 400V 3A general-
purpose silicon devices from my parts bin would make
suitable replacements, so I quickly substituted a pair of
new diodes.
Switching on the TV produced screen images for about
20 seconds until my replacement diodes got very hot, also
lost their smoke, then the set died again.
Sony, in their quest to minimise power consumption,
had specified high-speed schottky diodes for their power
supplies in the KD-65X7000Es, which meant my substitutes were not suitable. So I bought a strip of 10 schottky
diodes from Amazon for about $20 and replaced the two
faulty ones, as well as the other two that made up the bridge
rectifying circuit.
This time, the set sprang into life and continued
to operate satisfactorily. The new diodes were barely
warm. The 4K picture was crystal clear, with no screen
defects, and great audio – so I had acquired a marvellous 65-inch TV for about $4, plus another $15 for a new
remote control!
Unfortunately, the owner had discarded the mounting hardware for the set, so I had a bit more work to do to
make a frame to support the set from my old audio cabinet. The attached photo shows the setup, with the Jensen
X-125 at lower left.
Happy days.
SC
Rob Fincher, McCrae, Vic.
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February 2026 91
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