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SERVICEMAN’S LOG
Batteries, monitors, lights and audio
Dave Thompson is once again busy doing whatever he does when he
disappears: fighting an alien invasion, creating a new sheep hybrid, or
practicing his haka – we aren’t sure which, but it must be one of those.
Anyway, in the meantime, Bruce Pierson has been very busy in his shed
fixing everything that comes across his bench, so here are some of the
things he has repaired lately.
To start things off, my son asked me if he could borrow my battery charger because his had stopped working.
I asked him to bring it over and I could see that it was a
switch-mode type, which are sometimes tricky to fix, but
I said I would a look at it.
I started by removing the four Phillips-head screws on
the bottom and split the case apart. Thankfully, they didn’t
use ‘tamper-resistant’ screws as is so common these days!
I had a good look over the circuit board. All the electrolytic capacitors looked OK, with no bulging tops, so I turned
it over and examined the copper side with a magnifying
glass to check for dry joints, but there were none. In fact,
it looked as if it were quite new, probably because it was.
It was a change from the older items I usually work on.
I got out my ESR/Low Ohms Tester from Electronics
Australia, February 1996, that I built from a Jaycar kit. It
indicated that all the electrolytic capacitors were good.
This device has been very useful over the years for finding
faulty electrolytic capacitors that showed no external signs.
The MK II version of this tester was featured in the Silicon
Chip March & April 2004 issues (siliconchip.au/Series/99).
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Silicon Chip
Next, I got out my In-Circuit Transistor, Diode and SCR
Tester to start testing all the two- and three-legged semiconductors. I started with a diode, but the tester was not
working correctly. It was flashing very dimly and slowly,
then stopped flashing, with one LED lit dimly. It was a
sure sign that the battery had gone flat since I last used it.
I built it from a Jaycar kit of an Electronics Australia project from September 1983, and it has proved very useful.
When I tried to remove the 9V battery, the negative terminal came off the battery.
It took some effort to remove this detached terminal from
the battery connector, but I eventually got it off. With a new
battery fitted, I could continue testing. Nothing showed up
as faulty. I noticed that near the battery leads there was a
component that was likely some sort of SCR. I wondered
if it might be faulty.
I tested it, but no matter how I connected the leads from
the tester, it came up as an open circuit. Well, that must
be it. I used my 20W soldering iron to remove it from the
board and tested it again with the same result. Now I had
to identify it so I could order a new one.
The writing on the device was almost unreadable, but
I thought I could make out IRF724N. I looked on eBay for
this and found nothing suitable. A Google search for the
component gave many hits for IRFZ24N, so I guess what
looked like a 7 must have been a Z. I searched again on
eBay and ordered five from China for just over $5.
It took only 12 days to arrive. This is a 55V, 17A Mosfet so
I was surprised the original failed as it seems quite robust.
I soldered it to the board and clipped the excess leads off.
It mounts in the top-left corner of the circuit board, on the
left side of the battery cables.
I decided to test the charger before reassembling it. I
set the charger on the bench with a spare 12V SLA battery connected, plugged it in and switched on the power.
After a couple of seconds, the charging LED came on next
to the power LED, so I knew I could reassemble it and give
it back to my son.
I checked the Supercheap Auto website to see if this
charger was still available, but it was not. Similar chargers
cost between $60 and $100. My son has had this charger
for several years now (it came with the caravan he bought).
His caravan battery is charged by two solar panels, with the
charger being used to top up the battery when necessary.
Australia's electronics magazine
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The internals of the
Samsung SyncMaster
2253BW monitor. The
remains of the lizard
were very clearly
present when the back
was taken off.
It cost just over $1 to repair the battery charger, a considerable saving compared to buying a replacement charger.
Saving a ‘new’ SLA battery
I was sorting out some things in my shed when I came
across a new UPS box that had a brand new UPS in it. I
didn’t remember having this, so it must have been in the
shed for a very long time. I could tell by the weight of the
UPS that it had a battery in it, which was a bad sign.
These SLA batteries must be kept charged because when
the voltage drops below a certain point, they will refuse
to charge again. In that sense, they are worse than flooded
lead-acid batteries. Of course, car batteries should never
be in a situation where they are allowed to become dead
flat, as it shortens their life. Still, usually you can recharge
them if they go flat.
I took the SLA battery out of the UPS and tested the
voltage with my multimeter; sure enough, it read 0V. That
was a waste of a new battery. I was just about to recycle it
when I thought I would connect my SLA battery charger
to see if there was any chance it would charge. It wouldn’t
hurt to try.
I left the battery connected to the charger for a couple
of hours, but when I came back, the battery was still dead
flat. Just as I was about to put the battery into the scrap pile
again, I had a thought. I had nothing to lose, so I decided
to connect my car battery charger to it. I came back after
15 minutes and the ammeter on the charger showed that
the battery was charging.
That was unexpected, but it was a good sign that the battery might be able to be salvaged. I didn’t want to leave the
battery connected to the car battery charger, so I swapped
it for my SLA charger, and the charger’s LED turned red,
indicating that the battery was charging.
After several hours of charging, I switched the charger
off and got a 55W quartz halogen globe and tested the battery with it. The globe lit up at full brightness, showing
that the SLA battery had come good.
I had another old SLA battery in the scrap pile, so I
thought I would try charging it with the car battery charger, but it did not work, no doubt due to the age of the battery. Also, it had bulging ends, indicating that the plates
had deteriorated to the point of no return.
An SLA battery is only worth a few cents as scrap, but
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a replacement battery is around $40. So this experiment
was worthwhile.
Sometimes in a situation like this, with nothing to lose,
it pays to experiment. You never know when things might
turn out better than expected.
Samsung monitor reptile removal
I’ve had this Samsung SyncMaster 2253BW monitor for
many years. Previously it was in use in my back shed where
I used to do electronics repairs before I got my new electronics workshop finished last year. I used to work more on
computers and monitors, but now I mostly work on laptops.
A few years ago, I went to switch on the monitor and it
tripped the safety switch. I unplugged it and put aside. I
reset the safety switch, got another monitor, and continued
doing what I had been doing at the time.
I suspected that a gecko might have gotten inside the
monitor and shorted out something on the power supply
board. I had this happen to an Asus monitor a long time
ago. In that case, the fuse had blown and some tracks were
damaged from arcing, but I was able to repair it.
This monitor is a bit tricky to disassemble. I started by
unscrewing the stand/base, then I unclipped the front
screen surround. This gave me access to the two screws
that hold the stand stem on, so I could remove it. Then,
with the monitor face down, I could remove the back shell.
With the back off, I unplugged the front control cable.
There is a metal screen to remove, plus four plugs for the
high-voltage supply. I put some dots on them so I would
know which one went where, as I thought this might be
important. I now had the metal shell with the power supply board and the video board loose from the rest of the
Items Covered This Month
• A shopping list of repairs
• Lights out on a receiver
• Fixing the fan bearings in a gas heater
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
Australia's electronics magazine
July 2026 89
The garden lights at night and one of the working glass
solar panels.
monitor. And there I found what was left of the gecko.
After removing the gecko and cleaning the board, I could
not see any damage. There were no burnt tracks or any other
signs of damage, but there was a small area on the back of
the screen with a black mark where the high voltage had
arced onto the gecko. Maybe the gecko shorted things in
such a way as not to cause any actual damage. Here’s hoping!
I placed the metal shell with the boards in it on the concrete floor, plugged in a power cable and switched it on.
Nothing happened. There was no smoke or any other sign
of anything being wrong. Maybe I got lucky with this one.
I put the monitor back together loosely so I could test it
before reassembly.
With it facing up, I connected it to power and pressed
the power button on the front screen surround. The screensaver came on, indicating that the monitor still worked. I
reassembled the monitor and then took it into the house
and connected to my Linux laptop with a VGA cable. I got
a good picture, so the monitor had been restored to working order.
This time I didn’t have to actually repair anything, just
remove the cause of the safety switch being tripped. Good
thing we have a safety switch!
Garden light repairs
We have 50 garden lights around features in the front of our house and on the
side of our driveway. Some of these lights
need maintenance from time to time. I usually check them every so often to see if there
are any that aren’t lit when it gets dark. It had
been a few months since I last checked them,
and I found that 30 weren’t working.
The most common reason they fail is
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Silicon Chip
that the rechargeable AAA cell needs to be replaced. This
was the case with 27 of the non-working lights. I only had
21 rechargeable AAA cells in stock, so I had to order some
more cells on eBay. I usually get 24 at a time so that I have
a good supply on hand.
Another point of failure is the YX8018, which is a specialised, low-voltage solar LED driver IC used primarily in
solar-powered garden lights, lawn lamps and fairy lights.
It is a single-chip solution that manages battery charging
during the day and drives the LED at night, operating efficiently at the low voltages typically supplied by a single
1.25V NiMH rechargeable cell.
As with the cells, I was able to obtain replacement
YX8018 ICs on eBay.
Another point of failure is the colour-changing LED,
which I occasionally have to replace if one colour goes out.
I was also able to obtain these on eBay. It’s not very often
that I need to change one, though, as they last a long time.
The final point of failure is the solar panel, which is a
40 × 40mm glass panel. If this fails, the garden light is not
repairable, as I cannot find glass solar panels of that size
anywhere.
Similar plastic solar panels are available on eBay but
they cost more than a replacement garden light, and in any
case, plastic solar panels are lucky to last a year here in the
Queensland sun. The glass panels can last 10 years or more.
As for the other three garden lights that were not working,
two had a failed solar panel and one had a failed YX8018
IC. In the case of either component failing, the light will
either not work at all or be on all the time in bright light.
To find out which, I disconnect the solar panel from the
circuit board, set it under a bright light and connect my
multimeter to the wires.
These small solar panels deliver around 1.8V at
20-100mA to charge the AAA cell during the day. They
produce voltage even out of direct sunlight. They comprise three individual cells that generate around 0.6V each.
I replaced the two lights with failed solar panels and
repaired the last with a new YX8018 IC. Whenever I buy
a new garden light, I take out the AAA cell that comes in
it and I replace it with the much better one from eBay as
these cells keep the light lit for longer at night and also
have a longer life expectancy.
In the process of repairing the garden lights, I had to
reseal some holes where the wires from the solar panel
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siliconchip.com.au
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
Left: the standing spotlight, which was rewired so that it
had a longer cable, and did not need an extension cable.
enter the light, as some were not sealed correctly, allowing
water to enter the light. This resulted in a couple of battery connectors needing to be replaced; I used parts from
old lights that had failed solar panels.
In over 10 years, I have amassed 20 lights with failed
solar panels. I also replaced two glass bodies, as the water
had rusted the bottom screws, which caused the screws
to expand and break the glass. Sometimes a light may get
broken from another cause as well.
Simple headphone repair
My son brought me some headphones that had the cord
ripped off. He pointed out that there was a tiny piece of
red wire still attached to one speaker terminal so I’d know
which wire went where.
I got my 20W soldering iron out and plugged it in to heat
up while I prepared the wires for the repair. The wires
appeared to be cotton-covered, multi-core enamelled copper wire, so I used a lighter to burn off the cotton covering
and the enamel at the end.
I was then able to tin each wire, ready to solder them
back to their respective terminals on the speaker. I carefully soldered each wire to the correct terminal and put the
speaker back onto its bracket.
This was an easy repair that
only took me a few minutes.
I gave the headphones back
to my son and suggested that
they should be stored where
their cat could not find them
again, as it was fortunate that
the headphones had not been
ripped to pieces. If the cat had
another go at them, it could
end up a lot worse than just
the wires ripped off.
Rewiring a
standing spotlight
I’ve had this standing spotlight for several years, but
hadn’t used it. It had a short
cable with a footswitch,
which may have worked well
inside a house with the power
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points near the floor, but it was impractical in my workshops with power points above the benches.
I had been using it with an extension cable, but I decided
to rewire it to have a longer cable without the foot switch.
I looked on Jaycar’s website and found the exact cable I
needed, sold by the metre.
I worked out that I needed six metres, as the stand was
around 1.5m high and that would give me around 4.5m of
cable to reach a nearby convenient power point.
I knew I had a plug to suit this twin-core flat cable, as
I had planned to use it to repair a fan from the local Tip
Shop that someone had cut the plug off, but at the time I
could not find it. In the meantime, I had found it and lost
it again, but after a quick search, I located it and put it on
my workbench until the cable arrived.
When it did, I started by removing the two screws securing the shade and lamp holder to the stand. Then I fed some
cable up through the stand so I had working room to disconnect the cable from the lamp holder. With that done,
it was time to remove the old cable and run the new cable
through the stand and connect it at both ends.
After removing the lamp holder and the lampshade, I
tried pulling the cable through the stand from the bottom,
but it got stuck and I could not
pull it through. I suspected
that there might be a join in
the cable, so I unscrewed the
segments one-by-one and,
sure enough, there was a join
in the cable.
I cut the joint off the
cable and I was then able to
extract the old cable through
the segments and then
through the bottom of the
stand and out of the base,
ready for the new cable to
be installed.
I fed the cable into the
stand base from the bottom,
Australia's electronics magazine
July 2026 91
The JVC
receiver,
which
needed
tracks to be
bypassed
with wire,
due to
corrosion.
disintegrate is a mystery because they are on opposite ends
of the PCB. On close examination, it looks like the tracks
have oxidised in numerous sections. There is no visual
indication of burning or lifting as if it had occurred from
overcurrent heat stress.
Editor’s note: while those supply tracks carried an AC
voltage, there would likely have been a small DC voltage.
That, combined with moisture and acid from decaying
insects, is likely to lead to electrolytic corrosion. The solder mask is porous and doesn’t prevent the copper tracks
underneath from corroding away under these conditions.
Paul James, Kanwal, NSW.
Braemar gas heater fan bearing repair
but I found there was a plastic sleeve at the top of each
section that the cable was getting caught on. I fed the cable
through from the top instead, which proved to be successful. I screwed the segments together and then onto the base
as I fed the cable through.
Having connected the lamp holder and reassembled it, I
screwed the lamp holder and shade back onto the top flexible part of the stand.
The last job was to wire up the plug. A regular plug is not
suitable for this two-core flat cable because the cable hole
in the outer section of the plug is too big, so it was lucky I
still had this one that suited the cable. With the rewiring
finished, I tested the spotlight, and it worked as expected.
JVC RX 5032-VSL receiver repair
I was asked if I could do anything about the lights on an
amplifier/receiver so it could be used properly. The amplifier had no display and therefore couldn’t be readily controlled because there was no indication of volume settings,
radio stations or any other functions.
I completely dismantled the receiver and found that
numerous insects had entered the casing and had died
there or been scorched. On tracing the power supply circuit for the vacuum fluorescent display, it was clear that
no power was getting to it at all.
The AC voltage was coming out of the transformer at 5V
but not getting to the ribbon cable pins that supply the display. Testing with a multimeter on the PCB track from the
transformer and the pins showed an open circuit no matter where tested along the PCB track. The same thing was
happening on both outputs from the transformer.
The PCB track appeared to be a different colour from
the others and was unstable. Further testing on the track
revealed that it was all open-circuit.
The PCB track had to be bypassed with some wire to get
the transformer output voltage to the ribbon cable, maintaining the resistor in one leg of the supply.
During this process, I obtained a circuit diagram that
showed that the transformer was supposed to be supplying 15V AC, but all my measurements showed 5V AC and
the display worked after bypassing the faulty tracks, so I
guess that must be correct. Apparently, the circuit I found
is incorrect or for a different version because the transformer pinouts were different as well.
What really caused both of the supply tracks to
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Silicon Chip
When purchased and installed in 1982, our Braemar
gas wall heater fan was equipped with plain bronze bush
bearings. By 2021, not only had the bushes worn out, but
the bush at the fan end of the motor had worn a shallow
groove into the motor shaft.
Because there is only about a 10 thou (~0.25mm) clearance between the rotor and stator, the wear caused the rotor
to rub against the inside of the stator and emit a rhythmic
scraping sound, which steadily grew louder. By the winter
of 2022, the friction of the rotor against the stator became
sufficient to prevent the rotor from spinning.
Ball bearings should have been fitted when the motor
was manufactured. Provided that they were a reasonably
tight fit on the shaft, the ball race would rotate with the
shaft, and there would have been no shaft wear.
Clearly, something needed to be done, but what?
Braemar stated that they had no spare parts, but for
approximately $3000 they would provide and install a
whole new heater. Needless to say, that was never going
to happen for the sake of a couple of measly ¼-inch bearings. I explored other possible sources of new motors or
rotors, but couldn’t find any with a sufficiently long shaft.
The options then were:
Australia's electronics magazine
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1. Find and fit a new shaft. Perhaps a length of ¼-inch
(6.35mm) diameter silver steel rod or a drill blank would
do the trick.
2. Manufacture a new shaft from a suitable length of
hardened steel.
3. Purchase a replacement motor of suitable dimensions
but with a short shaft, and extend it using a collar.
4. Fill the grooves on the existing shaft, perhaps by metal
spraying.
5. Turn some new bushes from bronze bar or rod.
6. Fit ball bearings and fill the shaft grooves with epoxy
resin.
7. Fit ball bearings and fill the shaft grooves with epoxy
resin reinforced with fine steel filings. Such mixes are
available commercially, but anyone with some scrap metal
and a file can make their own (I once drove from Oslo to
London after repairing a chewed-out rear axle spline in
this manner).
Option #6 seemed to be the least expensive and most
expedient. Even though epoxy is a relatively soft material
compared to steel or chrome, it wouldn’t be subjected to
wear so long as the shaft and inner race rotated as one.
Because option #6 was likely to involve a delay of several
days while suitable bearings were delivered, I attempted a
temporary fix using the existing bush bearings by filling the
groove worn into the shaft with epoxy mixed with graphite.
In theory, the graphite would provide a low-friction bearing surface while the epoxy held it in place. Unfortunately,
the epoxy collapsed after about four days, bringing the fan
to a halt once more. Curses!
By the time the ball bearings arrived, I’d refilled the
groove worn in the shaft with plain epoxy and, using nothing more than a fine file, reduced the filler to the same diameter as the shaft. Voilà! The bearing slid on neatly with a
small interference fit.
Moreover, the ball bearing width proved to be equal to
that of the original bronze bushes, so the shaft position and
end play were no different once the original spacer was
installed on the shaft between the rotor and fan end bearing.
Having measured the bearing outer diameter, I made
ready to turn a suitable spacer ring to support it inside the
motor housing. Then I had a brainwave. Had my old friend
Ian not recently gifted me a box of various-sized O-rings?
Maybe the box might yield a couple sized suitably for this
purpose. Indeed, I found four.
There was only space for one per bearing, leaving the
possibility of the O rings migrating to the outer end of the
bearings and releasing them. I needed some annulus-shaped
packing spacers that would slip over the bearing yet fit
inside the housing.
After rummaging through my box of washers and finding
nothing suitable, I decided to experiment by cutting some
thin cardboard packing washers. After all, there was no
more danger of the cardboard burning than of the wiring
or plastic formers within the motor. I could always make
metal versions later if this worked.
Work it did, and wonderfully so. The fan is silent and
rotates with a vigour as never before. Whereas we habitually
ran it at the medium speed setting, we now use only the
low speed setting. It has been running this way for a couple of years, and I’ve never needed to replace the O-rings
or cardboard washers with anything more substantial.
SC
Ron, via email.
siliconchip.com.au
Australia's electronics magazine
July 2026 93
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