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SERVICEMAN’S LOG
Another mixed bag of bits and bobs
Dave Thompson recently surprised us by visiting Australia. It was such
a surprise, we didn’t know he was here! Having recharged his batteries,
he’ll be back in July. So, for now, here are some stories from our readers.
Mystery amplifier toroidal transformer replacement
The mains light-bulb limiter is not a new idea, but not
everyone is aware of it. My version is the simplest, comprising a 100W 230V incandescent lamp (these are getting
scarce) mounted in a batten holder screwed to the wall
above my bench. This is wired with a piece of two-core
mains flex to a PDL40A Interrupted Phase Tapon Plug.
This means that any appliance plugged into the Tapon
has the lamp in series with its live connection. I leave the
Tapon plugged into one outlet of a power board, and I can
choose to plug the appliance under test either directly to
the mains or via the Tapon. I use an inexpensive power
meter to measure the mains voltage and the current
drawn by the test load.
Turning to the repair in question, a PA speaker had
blown its mains fuse, so after fitting a replacement, I
plugged it in via the lamp limiter. I expected to see the
lamp briefly lighting brightly, then fading to a dim glow.
This is because the amplifier main capacitors charge
when power is first applied, drawing a large initial current, which then subsides.
However, the lamp lit up at full brightness and stayed
that way. If I had plugged it straight into the mains, it
would have likely blown another fuse. There must have
been a heavy short circuit somewhere in the amplifier.
I dismantled the amplifier module from the cabinet and
noted a large toroidal power transformer at one end. The
secondary wires were easily identified and fitted with
Faston connectors, allowing me to quickly disconnect
them. When I plugged it back into the Tapon, the lamp
immediately lit at full brightness again.
That indicated the transformer was the likely culprit,
but to be sure, I disconnected the transformer primary
and tried again.
This time, the lamp didn’t light at all. So a new transformer was required, but it had no markings on it to tell
me what the secondary voltages should be. A label on
the back panel told me the total power consumption was
160VA, so I needed a 160VA transformer with a 230V
The original transformer
(above) and replacement
(below).
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primary and a centre-tapped secondary of unknown
voltage.
I had a schematic of this unit, but there was no mention of the transformer voltage. However, someone had
written 35V next to the DC rails. That seemed a little
high to me, so I looked at the main capacitors on those
rails and found they were only rated at 35V. The actual
rail voltage would be less than that.
The amplifier uses LM3886 power amplifier ICs, so I
consulted the datasheet. This gives different rail voltages for 8W or 4W loads. The woofer was a 4W unit, and
the datasheet said the rail voltages should be ±28V. That
would suggest the transformer secondaries should be
roughly 20V AC.
A look at the selection of 160VA toroidal power transformers available from my regular suppliers showed two
contenders: 18-0-18V or 22-0-22V AC.
From experience, I know that a transformer rated at 18V
will deliver closer to 20V with a light load because it is
designed to deliver 18V at its full rated load. I selected
the 18V unit and, when it arrived, I was surprised to find
it was somewhat larger than the original. I fitted it to the
chassis with a bit of fettling and wired it up.
When I applied power again, all was well and the DC
rail voltages measured a touch over 28V DC.
I should mention that the light-bulb limiter can give
tricky results with appliances with switch-mode power
supplies. Most are OK, but some can draw a lot of current at startup, lighting the lamp and lowering the voltage
to the power supply, which may subsequently not start.
Not long after that repair came another, this time a
wedge floor monitor made by the same manufacturer
and using similar technology. Only this time, the woofer
amplifier was a discrete design with a higher power output. The customer said there was a crack sound, and the
HF horn stopped working.
I initially powered the box through my light-bulb limiter; again, the lamp came on at almost full brightness
Items Covered This Month
• Mystery amplifier transformer replacement
• A curious remote control problem
• HP 8660D signal generator repair
• Arlec NL0009 LED Night Light repair
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
and stayed that way. The customer said it was still working, so I held my breath and plugged it directly into the
mains. It came on and, as described, the woofer was
working but not the horn.
A quick resistance check of the horn driver revealed
it was open-circuit. Connecting my ‘scope to the output
of the horn amplifier explained why. There was a solid
-30V across the horn, meaning the IC amplifier driving
it had failed and had taken the horn with it. If I had just
replaced the horn driver, the new one would have burnt
out at switch on.
After replacing the IC (LM3886), I tried again with the
light-bulb limiter, and this time the bulb came on bright
and then faded to a dim glow as expected. This suggests
that the faulty IC was also drawing a lot of current; I
think if it was powered up for any length of time, there
would have been smoke.
Paul Mallon, Christchurch, New Zealand.
A curious remote control problem
I had noticed that our air conditioner remote control was working poorly. It would control the AC, but it
seemed less sensitive, and the AC unit did not display
the set temperature. I have a separate control for each
room, so tried another one with no better result.
That evening, I also found that the LG TV was responding strangely. I changed the batteries in the remote and
even tried a second one with no change.
The next morning, I tried using the sound system with
a new (replacement) remote control. This was also acting strangely; since the batteries were low, I replaced
them. I then had the bright idea of checking the sound
system remote itself and found that it was continuously
transmitting.
Opening it and carefully reseating all the buttons
stopped that, and now everything else worked properly.
So, although the controller was transmitting codes not
recognised by the AC and TV, it was enough to interfere
with both systems.
Graham P. Jackman, Melbourne, Vic.
HP 8660D signal generator repair
I went out to the radio shack intending to check some
VHF receivers using my Hewlett-Packard 8660D signal
generator. However, my effort was short-lived – the sig
gen didn’t want to produce any useful output.
Of course, the HP that built this sig gen is very different from the HP we know today as an IT company. The
test and measurement arm of HP that created the 8660D
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June 2025 89
was spun off from the IT company many years ago and
became Agilent, later renamed to Keysight.
When it was released in 1971, the 8660 was truly
‘bleeding edge’; it was the first fully synthesised sig gen
built by HP. Although HP built frequency synthesisers
before the 8660, they lacked the modulation capability
and a wide range of calibrated output levels.
The 8660’s specifications were impressive. In its early
form, it offered 0.01MHz to 110MHz in 1Hz steps, AM or
FM modulation, and an output from +10dBm to below
-140dBm. Its output was also clean, with all in-band
unwanted (spurious) outputs at least 80dB below the
level of the wanted frequency; a real achievement. Truly
impressive for the time!
Add two front-panel plugin bays for a modulation section (with various options available) and the output section (again, different modules available) and it was a very
flexible design. It also had an internal plug-in bay for a
“Frequency Extension Module”, which was required for
the later 1300MHz and 2600MHz versions.
The one specification that was a bit below par was
phase noise; the analog HP 8640B signal generator stayed
king of the phase noise heap for many years after the
8660 was released. Phase noise is the wideband noise
created by all oscillators, with some designs much better than others. Still, the 8660 was still very usable for
most purposes.
All of this did not come cheap or small. Despite being
designed in the early 1970s, the 8660D was still on sale
in 1990. The list price in 1990, for the 2.6GHz version
with plugins, would not leave you with much change
from US$40,000. But you got a lot of hardware for your
money – a 4U (about 175mm) high 19 inch rack-mount
box over 500mm deep and weighing about 30 kg.
So, when I switched it on and no signal appeared, what
to do next? My first check was with a spectrum analyser
and frequency counter, which confirmed that with the
8660 set to a nominal frequency in the VHF range, it had
an unstable (frequency varying) output at a few MHz.
Fortunately, HP instruments came with excellent documentation, usually including an operations and service
manual with full schematics, part layouts, fault-finding
guides and parts lists down to individual components.
Scanned versions are often available online.
One useful source of info on the higher-end HP equipment is the Hewlett Packard Journal. Although essentially a sales strategy, the HPJ often had articles written
by the project development teams about the high-end
new equipment they had developed. For the 8660, the
March 1971 and December 1971 HPJ issues both had very
useful information, one about the 8660 mainframe, the
other about the plugins.
There are two basic fault-finding options in a complex
system such as this, where no functional block stands out
as the most likely to create the problem. One is to start
near the signal source and work through the instrument
to locate where the correct signal disappears, or work
backwards from the output and find where the fault stops.
Starting at the source was not attractive. It is a 100MHz
master oscillator which is phase-locked to a reference
oscillator at 5MHz or 10MHz, which can be either internal
or external.
Many different signals are derived from the master
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oscillator by frequency division or multiplication, to
provide the reference signals for the phase-lock loops –
7 PLLs in the mainframe, plus several more in the Frequency Extension Module and in the output plugin. That
means a lot of signal paths to check, including several
complex programmable frequency dividers.
Starting at the output and working back looked a lot
easier. The output plugin module receives only two signals from the Frequency Extension Module: one tuning
from 2.750GHz to 3.950GHz in 100MHz steps, the other
tuning from 3.950GHz to 4.050GHz in 1Hz steps. The
desired output frequency is the difference between these.
A fault found here on one signal would immediately
provide a path to further investigation ‘upstream’.
Although a service manual is available for the output
plugin, there is none online for the Frequency Extension
Module, and in any case, the Frequency Extension Module is basically impossible to test without special (and
unavailable – of course!) ‘extender’ cables. If the fault
was in one of these modules, the instrument was probably
a write off. So, trace backwards from the output it was.
I just needed to locate the relevant connections and
check with a spectrum analyser to see if the expected
signals were there. The instrument is a maze of cable
looms carrying various signals; most of the cables are
terminated with special-purpose plugin connectors that
have both coaxial and standard connections – which are
inaccessible with modules installed in the chassis. Sigh!
As it happened, the two required signals were actually
on SMB connectors, so it was only a few minutes to make
a suitable adaptor cable and have a look with the spectrum analyser. Lo and behold – one signal was absent.
So, the fault was probably not in the output plugin module – so that was one critical module cleared.
The Frequency Extension Module has four RF signals feeding into it, all via a multi-way connector. After
a bit of fiddling, I was able to make a cable that kind-of
mated with the coax connectors in the multi-way plug,
with the Frequency Extension Module unplugged (and
hence inoperable). Another test with the speccy showed
the reference signals to the Frequency Extension Module were not present.
Australia's electronics magazine
siliconchip.com.au
So the Frequency Extension Module was probably
OK, too. Big sigh of relief! Now I had a new place to
look – the circuits that generate the reference frequency
signals used by all the phase-locked loops.
The 100MHz master oscillator is used to generate
500MHz, 100MHz, two 20MHz, two 10MHz, 2MHz,
400kHz, and 100kHz reference signals. These are easy
to check in what’s called the A4 assembly, which has all
the circuitry to generate the reference signals.
Most, but not all, reference frequencies were MIA, so at
least the master oscillator was operating, but the circuits
to generate most of the reference frequencies weren’t.
Then I spotted some greenish corrosion on a small area
of the “A4A4 reference loop and dividers” circuit board.
Closer inspection showed that an electrolytic capacitor
used as a bypass on the -10V power rail had leaked onto
the board and the electrolyte had eaten a couple of power
supply tracks. Bingo!
After that, it was easy. Clean up the board, replace the
missing tracks with copper wire bridges, a new capacitor, and we were in business. Or so it seemed.
As a final check, I hooked up the sig gen output to my
frequency counter, which is locked to a GPS reference.
That showed the sig gen was putting out a signal significantly low in frequency, which drifted in frequency as
I watched. Bother! Was there another fault with one of
the phase-lock loops?
Then the penny dropped – the sig gen was using its
internal reference, an ovenised crystal oscillator, very
likely the venerable HP 10544A or something similar.
This was drifting low in frequency as it came up to temperature during its warm-up phase before settling to
something very close to the correct frequency.
Previously, I had always used the sig gen with an
external reference from a GPS-derived 10MHz frequency
source, so I never saw this behaviour. So, with relief, I
decided it was all good!
John Morrissey, Traralgon South, Vic.
Arlec NL0009 LED Night Light repair
We have two separate car garages and, a few years ago,
we decided that a motion sensing night light in each
garage would be ideal to help find our way to the light
switch or door when we come home at night. So we purchased plug-in Arlec NL0009 PIR motion sensing LED
night lights from the local hardware store and installed
one in each garage.
These are low-cost plug-in devices and worked very
well until a year or so ago, when the first one became
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
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Australia's electronics magazine
June 2025 91
faulty. It was still functioning, but the light output had
become very dim, so I accepted the challenge to see if it
was easily repairable at minimal cost. These units come
apart easily with the removal of four small Phillips-head
self-tapping screws to reveal the PCB.
My first thought was it could be a problem on the supply side from the incoming 230V AC to the electronics.
I could not find a circuit diagram for these units, but
inspection of the PCB showed the power supply to be
fairly conventional.
This consisted of a 330nF 275V AC rated X2 capacitor paralleled by a 390kW resistor and connected in
series with a 47W resistor (on the underside of the PCB)
between the incoming 230V AC supply and a bridge rectifier, BD1. Across the DC output side of this rectifier is
SMD capacitor C14, plus C15, a 220uF 35V electrolytic
(on the underside) and a SOD-80 type zener diode, ZD1.
This provides a voltage-limited, filtered and regulated
DC supply to power the night light electronics and the
white high brightness LED lights.
I first checked the 330nF X2 capacitor as I recalled one
failure mode of these metallised film ‘safety’ capacitors
is to lose capacitance over time due to internal partial
discharges, which progressively degrade the metallised
film.
I measured the capacitance of the X2 capacitor with
my DMM and found this to be about 230nF. This was
significantly below its labelled value, and would certainly explain the diminished light output from the
unit. I replaced this faulty component with a new
330nF X2 275V AC capacitor and its full light output
was restored.
About six months later, the second night light failed,
but this time with no light output at all. I opened up the
unit and firstly checked the 330nF X2 capacitor, finding
its capacitance to be about 320nF, which was acceptable.
I next used my current-limited DC bench supply to
apply voltage on the AC (input) side of BD1, checking
both polarities. Voltage measurements indicated about
1.6V across the bridge input, for either polarity, before
a significant current draw started. This seemed to be
indicating a short circuit somewhere on the output side
of the bridge rectifier; 1.6V is approximately equivalent
to the sum of two forward-biased diode voltage drops
in the bridge.
Zener diode ZD1 seemed to be the most likely culprit, followed by the two DC filter capacitors. I removed
ZD1 from the PCB and, on testing, I found it to be pretty
much a dead short circuit. Assuming the zener diode to
be the only faulty component, the next challenge was
determining what voltage it should be.
The zener had what appeared to be one green band
with no other markings. A quick online search was of
little help, so with no zener in the circuit and the light
sensing photodiode (photo 1) shaded with a small piece
of black tape, I decided to apply a current-limited DC
voltage to the output side of the bridge rectifier.
I slowly increased the voltage while moving my hand
over the PIR sensor, and at about 22V, the LEDs started
to glow. Further increasing the voltage to about 28-30V
resulted in a LED brightness level of about what I thought
it should be.
As a further check, I decided to test, in a similar way,
the previously repaired Arlec unit from the other garage.
This unit still had the original zener diode installed and
showed the voltage developed across the zener to be
about 30V, so that was good confirmation.
As I didn’t have a SOD-80 type 30V zener diode on
hand, I decided to try two series-connected DO-41 zeners of 13-15V, hoping this would be good enough. These
diodes were easily installed sitting just above rectifier
BD1, and the repair proved to be very successful.
While I was at it, I decided to also replace the original
X2 capacitor just in case it was heading the same way as
the original X2 capacitor in the other unit.
So, with a little effort and replacement of a few lowcost components, both night lights are continuing to provide their helping glow when we come home at night.
SC
Stephen Denholm, Tranmere, Tas.
One of the
repaired night
lights.
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The replacement
grey 330nF X2
capacitor is much
larger than the
original but it
still fits.
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June 2025 93
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