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SERVICEMAN’S LOG
Designing for unrepairability
Dave Thompson
A lot of equipment these days is designed to be compact and easy to
assemble, but little attention is given to repairability. That’s why so many
devices are essentially disposable. There’s no information like circuit
diagrams or repair manuals available, so once something goes wrong, in
the bin it goes. It’s sad.
I
’ve mentioned before that I get a lot
of random devices into the workshop for repair. Once people hear I
can do this sort of thing, they all seem
to pour out of the woodwork with
all manner of strange and wonderful
things for me to fix.
One of the problems I have with
this is that many of these devices are
no longer supported, built to fail and
designed not to be repaired, or simply not worth the considerable time
it would take to fix them.
The other day, a guy brought in
a hand-held Garmin Rino 650 GPS
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transceiver. This is a very handy unit
because not only is it a fully-featured
satnav system, it is also a two-way
radio, so hunters who have other
compatible transceivers can talk to
each other over quite long distances
in the bush.
These devices have a touchscreen
menu system and a PTT (push-to-talk)
button on the side of the rubberised
case, so they work much like the typical ‘walkie-talkie’ type devices we all
know and love.
The problem with this one was that
there was no sound output, so while
it can still be used as a standard navigation system, there were no audio
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prompts and obviously no radio transceiver function.
These devices are designed to be
rugged. They use heavy rubberised
plastics and lots of rubber bungs and
stoppers to provide basic weatherproofing. Pulling them apart isn’t too
onerous, with the usual long Torx-type
screws (which require the exact driver
bit or they aren’t going anywhere) and
the increasingly typical hidden screws
buried beneath barely-removable case
flashings.
If one isn’t thorough, trying to pry
apart a case that still has screws holding it together can end up a real mess,
especially if one isn’t having a good
January 2022 89
day and the red mist comes down in frustration!
With all the screws removed, the two halves of the case
separate relatively easily, but then the space is so tight that
you have to hold your tongue one way while the planets
align before the board assembly can be eased out. There
is literally only one way it can come out, and finding just
where that sweet spot is can be maddening.
Once I got the board out, it was pretty obvious I was not
going to be able to do much with that part of it unless the
problem was caused by something simple like a blown or
faulty speaker. The speaker was one of those super-thin
permanent-magnet types, about 25mm in diameter and
plastic-welded into the front of the case.
There was no physical wiring connecting the speaker;
the board simply pressed against it, and a couple of tiny
gold spring contacts on the PCB rested against the speaker’s terminals.
I guess with everything crammed in so tightly, this system does work well, but I’d imagine any moisture that
gets inside might interrupt this type of connection, so I
resolved to take that into account as well.
I decided to check the speaker first. My trusty multimeter could handle this with a quick touch to the speaker
terminals with the meter set to x1 on the ohms scale. A
click from the speaker told me it was working, which, to
be honest, made my heart sink a little because I was hoping it would be one of those silly fixes that resolves everything with a minimum of fuss and expense.
But no. There was obviously something further up the
audio chain that was stopping this from making noise. As
is usual in these situations, I hit Google to see if I could
locate any circuit diagrams or schematics that may help.
I found nothing but a wealth of misinformation. However, one theme kept cropping up: that on this model, it
is easy to mute the output by accident whilst perusing the
menu system, so many people had resolved the no-sound
issue by simply un-muting the audio.
I reassembled the GPS to the point that I could fire it
up and go through the menu options on the touchscreen.
The sound was not muted, which was disappointing, but
there was also an option to set the handset to vibrate. I
had seen the tiny vibrator motor mounted on the circuit
board, so I knew it had that feature available.
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I set that to on, so at least there was some haptic feedback when something happened, though that wasn’t going
to help get the two-way radio working...
Breaking it down the second time wasn’t as finicky a
job as the first time, so that was something. But trying
to track anything back from the speaker side was a nonstarter. The multi-layer PCB was stacked with the smallest
SMD components I’ve seen for a while, and though some
did have numbers printed on them, I could find nothing
about what they were.
Even if I could find a replacement, removing them
would require specialised tools that I don’t have, and if I
tried to do it, I’d likely have just damaged the board further. So, this was one that I couldn’t help with.
Garmin no longer runs a swap-out refurbishment program for this model, so they were no help. While I did
check the usual auction sites for spares and replacement
units, I could only find models being sold for spare parts,
and they could very well have the same problem as this
one – the vendors couldn’t tell me what had gone wrong
with them.
At almost half the price of a new unit, buying dead
handsets in the hope that something might work was just
not feasible (or sensible). The owner was philosophical
about it; at least we’d had a look and determined it wasn’t
worth pursuing. He’d still use it as a GPS but would have
to do without the radio/audio side of it.
Next!
Another client brought in an old ’70s clock radio. It had
been in the family for years, and though it worked, one
of the red seven-segment LED displays had faded enough
that it was difficult to read the time.
This is a classic example of whether to repair or not,
and why each case should be taken on its own merits. The
clock radio had been bought for the current client back
in the day by his dad, and so it had a lot of sentimental
value. He had used it in his workshop for many years and
wanted to see it going properly.
I advised him that I could likely fix it, but he might
be looking at way more than a replacement clock radio
from some big-box store might cost. He was OK with that
because the sentimental value was greater than that for
him. I told him I’d see what I could do.
Working on these older devices is so much nicer than a
lot of today’s stuff: plain screws, simple engineering holding it all together and basic analog components with designations printed on them. Almost anything inside it could
be repaired, or even fabricated to fit if that’s what it takes.
This clock just had a single dim display from the four
onboard, and I guessed that it had simply faded with age,
as many LEDs of all types of this era do. The big question
was what type of display it is and the pin configuration,
because I literally have a parts drawer full of reclaimed
and NOS (new old stock) red seven-segment LED displays, and I felt confident one would fit in this old-timer.
I’ve said before; I’m not exactly a hoarder – at least not
to the extent I have to sleep standing up in the laundry
because all the rooms are stacked floor to ceiling – but my
workshop is quite ‘busy’, with parts drawers and shelves
groaning under the weight of stuff I’ve accumulated over the
last 40 years or so. That’s not including all the other things
I inherited from dad’s very similarly-appointed workshop.
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The new display was a little brighter, but not too bad. I
guess I could have installed a resistor in the ground line
in an effort to dull it, but I thought that once the plastic
front was in place, it would look OK.
I was right; once reassembled, the red plastic cover the
LEDs shone through, which was a bit faded and scratched
itself, tempered any bright spots on the new display, and
it looked just as good as the others.
The customer was pleased, and I’m trimming down my
component stocks the right way, one at a time.
On the slow boat from China
The rationale is that if I come across a new-old-stock
seven-segment display, I’m not about to throw it out just
because I’m running out of room, so it gets squeezed into
the drawer with the others.
While there isn’t a huge call for components like this
anymore, I could almost guarantee that if I did have a
colossal clean-out and biffed a lot of this stuff away, the
very next day, a job would come in that requires something I have just binned.
This clock-radio job has proven that it would have been
folly for me to throw these displays away because, as luck
would have it, I had several that could do the job. My main
concern was that if I fitted it successfully, this ‘new’ one
would be much brighter than the remaining original displays. As I didn’t have four the same, I couldn’t replace
them all. Still, I’d cross that bridge when I got there.
It was a bit tricky to manipulate the various PCBs into a
position that I could de-solder the dud display. The separate
boards were all linked together using that multi-stranded,
hard plastic insulated joining cable. It’s great stuff for a
strong interconnecting joint, but over time it gets brittle and
breaks easily. If I did break a link, I could always replace it,
but it’s better not to bend these old parts around too much.
The smell of the old solder brought back memories of
watching dad in his workshop when I was a little kid; it’s
strange how some odours stay with you. It’s likely seriously unhealthy, with all the fumes that come off when
heated, but it smells of home to me.
Getting the old dim display out was easy; I just wiggled it free after removing all the solder. The PCBs are
pretty hardy from those days, but like all electronics,
excess heat can do a lot of damage. So I just took care
not to overcook it.
I lined the new one up with the others and soldered
it in – it was really that simple. I flexed the boards back
into their original positions and sat it all carefully on the
bench before plugging it in and lighting it up.
siliconchip.com.au
You might recall a story a while back about an electric bike that I couldn’t finish repairing as I was waiting
on parts from China (June 2021 issue; siliconchip.com.
au/Article/14895). More specifically, I was waiting for a
new speed controller, because the old one had gone up
in a puff of smoke.
The problem was that I didn’t know if it was just the
controller that had failed, or whether the motor assembly built into the back wheel had shorted and burned
things out, or both. The controller was far cheaper to
replace than the wheel/motor assembly, so that’s the
bit I bought first.
I’d sourced one easily enough, as they appear to be
at least partially standard devices, but it took forever to
get here. When it did arrive, I installed it – thankfully,
most of the connections are also relatively standardised
– though I’d taken lots of photos before I pulled the old
one out as a precaution.
I charged the battery, which had been sitting for a while
and was discharged, and when all was ready, turned the
key and wound in a bit of throttle. In a flash, the new
controller was toast.
As I’d already previously checked the external wiring to the motor for obvious shorts between themselves
and to ground, I thought nothing was apparently wrong
with it. Still, without a compatible controller, I couldn’t
check it properly.
Therefore, the controller was intended to be a sacrificial lamb and did its job by telling us that there was no
point in carrying on and sinking even more money into
it. It was a shame, really, as it was a cute little thing and
not cheap to buy in the first place.
Last call
And finally, I had a guy bring in a PCB from a heat
pump compressor. These are pretty large, and he said no
one in town is repairing them anymore after a well-known
repairer shut up shop due to the pandemic.
Items Covered This Month
•
•
•
•
The art of unrepair
Macbook Air repairs
Repairing a double-clicking computer mouse
Replacing damaged varistors in two Panasonic
microwaves
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Australia's electronics magazine
January 2022 91
I know next to nothing about these
things, but how hard can it be? Circuit diagrams for common models are
widely available for service guys, and
the bloke (an installer/engineer) said
he could get a circuit if I needed one.
The fault was that the compressor
motor no longer ran, and he suspected
the motor driver section of the PCB had
failed. To start with, I asked him if he’d
tested the motor itself. He hadn’t but
claimed not many fail, so it was most
likely the board.
He left it with me, and I got out the
magnifying glass to see if I could find
something obvious. I could see no
burned areas and there was no acrid
‘dead component’ smell, so I doubted
this was the problem.
There were two onboard fuses,
though, so I checked them. One was
blown. I replaced it with one of the
same specifications and called the
installer chap to say there was nothing obvious here.
He went back to the house and
pulled the motor, bringing it straight
around. It was shorted every which
way I could measure it according to
my meter, so that was likely the problem. Whether it had smoked the PCB
itself was anyone’s guess.
But again, it is way cheaper to
replace a motor than a PCB in these
units, so he took both away and
installed a new motor, wired in the
old PCB and voila! The thing fired up
and is still running well today.
It just goes to show that sometimes
the simplest things can go wrong,
but our tendency to over-complicate
things can point us off in the wrong
direction.
He cursed himself for not checking
those onboard fuses instead of wasting
time taking the board out, but he made
his assumptions on his own experiences. If he’d tested the motor, he’d
have found the fault straight away, so
I can be sure that’s what he’ll do next
time. Either way, it was a super-easy
fix for me, and everyone was happy.
Macbook Air repairs
B. P., of Dundathu, Qld previously
wrote in to describe several MacBooks
that he brought back into service. Well,
he’s up to it again, this time rescuing
some MacBook Airs from the rubbish tip...
Some time back, a friend gave me
several MacBook notebooks. I was able
to repair three using parts from those
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and others that I already had. There
was also a MacBook Air, but I’d been
unable to test it because I only had
Magsafe 1 chargers and the MacBook
Air uses a Magsafe 2 charger.
More recently, I was given another
MacBook Air notebook, but I still
didn’t have a Magsafe 2 charger. Now
I had two of these MacBook Air notebooks and no way to test them. I’d
previously looked into the price of a
charger, but as they were around $40
or more, I didn’t want to spend that
sort of money without knowing if these
notebooks even worked.
I decided to look on eBay for a
replacement Magsafe 2 cable, and I
found one for $11.95, so I ordered
it. When it arrived, I dug out a 14.5V
charger with a Magsafe 1 cable, and
I cracked the charger apart using circlip pliers. One side of the shell came
off fairly easily, but the inside of the
charger proved challenging to get out
of the other half of the shell.
After I managed to remove it, I desoldered a wire and removed the copper
wrap. I was then able to desolder the
old cable and solder in the new one.
Then I refitted the copper wrap and
re-soldered the wire, and put the charger back together. The case clipped
back together nicely, without needing to glue it.
I grabbed one of the notebooks and
connected the charger to it. I waited
a minute and then pressed the power
button. I heard the familiar Mac boom,
so that was a good sign. The MacBook
loaded up with the previous user’s
account without needing a password,
but something wasn’t right. There was
no dock.
Then I discovered that the keyboard
and trackpad didn’t work, and I wondered if they had been disabled, so I
decided to boot from a USB installer
and check.
I had an earlier version of Catalina
on a USB, so I’d use that for now and
update it later. I pressed the Option
key and got the option of booting from
the HDD or the USB drive. The trackpad now worked, so I chose the USB
installer. I returned later, but now
the keyboard and trackpad no longer
worked; they were obviously faulty
and only worked intermittently.
I put this MacBook aside and
grabbed the other one to check it. Once
again, it started up, but I got a folder
with a question mark in it, indicating
that the eSATA SSD had either been
wiped or removed, so I booted from
the USB installer. There was still no
HDD present, so I guessed it had been
removed.
I took the back off, but I found
that the SSD was actually present. I
removed it and replaced it and tried
again, but it still didn’t show up. I
suspected it might be faulty, so I took
the back off the first MacBook Air,
removed the SSD and installed it in
the second MacBook. But it still didn’t
show up; I knew it was good, which
meant there was a fault with the motherboard.
I decided that the best option was
to swap the good motherboard from
the first MacBook Air into the second
MacBook Air. But this second MacBook had been dropped and there was
a significant dent in the front righthand side of the base and the lid, as
well as the base being bent where the
left USB port is, and the lid would not
close properly.
The other shell was in much better
shape, but I didn’t want to swap over
the keyboard, which is a massive job.
From what I’ve seen on YouTube videos with MacBook repairs, the keyboards are held in with a million tiny
screws, so I would have to repair the
damaged case.
I managed to tap the front corner
of the top case back into shape and
straighten the bent area at the USB
port, but I didn’t want to try to fix
the lid, as I could risk breaking the
screen. Instead, I would swap over
the good lid.
I started by dismantling the first
MacBook with the working motherboard. I removed the battery, then the
motherboard. I put the battery, motherboard and back of the shell aside to
Servicing Stories Wanted
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column? If so, why not send those stories in to us?
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Left: the left-most charger is a
Magsafe 1, while the one on the right
is Magsafe 2. The Magsafe 2 charger
uses the same pins, but has a slightly
longer connector,
fit to the repaired case. The reason for
using this back is that it has the correct
serial number of the motherboard on
it. I’d use this battery, as it was already
fully charged, and I knew it was good.
I disassembled the second MacBook
similarly, then swapped in the good lid
and fitted the good parts. Now the lid
closed properly after the shell repair.
I also put fresh thermal compound on
the heatsink and cleaned the fan at the
same time. For the moment, I just sat
the back on, in case I had to do anything else inside, and I turned it over
and connected the charger.
The MacBook started up, and this
time, all was well with the keyboard
and trackpad and I finished the installation. I decided to check for updates
and was offered the latest version of
macOS as an upgrade.
The download finally finished, so
I copied the installer to an external
hard drive, and I also copied it to a
folder on the desktop before running it.
After some time, it was installed and I
was greeted with a terrible wallpaper,
which I quickly changed to the Big Sur
photo after I logged on.
Further testing indicated that this
MacBook Air notebook was working
correctly, so the $11.95 investment for
a replacement Magsafe 2 cable was a
good move. I screwed the back on permanently, gave it a quick clean and it
was complete.
This was a successful exercise in
taking two unusable notebooks and
making one good one. I don’t yet
know if the leftover parts will be of
any use, but I have kept them in case
I get another broken MacBook Air in
the future.
When I’d had the other MacBook
Air apart, I could see some corrosion
around the connection for the trackpad, so that explained why it didn’t
work reliably. It looks like someone
had spilled liquid on the trackpad,
which had seeped through and got
into the connector. I haven’t looked
into it any further to see whether that
damage is fixable. It might be.
Apparently, the small chip in the
trackpad cable also controls the keyboard, explaining why both had
stopped working.
Working on Mac computers and
MacBook notebooks is vastly different
to working on PCs and Windows laptops. Mac computers and Macbooks
need a lot more different tools, and
they are a lot more compact.
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Below: the Macbook Air opened up,
so that the motherboard could be
swapped.
Australia's electronics magazine
January 2022 93
Repairing a computer mouse that double-clicks
D. S., of Maryborough, Qld made a similar repair to our
own serviceman, who described fixing a computer mouse
in the May 2021 issue...
Dave’s mouse repair story made me chuckle. A couple
of weeks ago, I was in a similar situation. A young fella
had a problem with his mouse; apparently, it was double-clicking on the right mouse button whenever it was
pressed. This, I was told, was “not a good thing when facing off with opponents in various online games”.
I asked if he had played with any of the settings in the
PC or the mouse’s installed software. He said he hadn’t,
and without the PC, I had to take his word for it. I did ask
if it was worth repairing, given that the repair might cost
more than a new mouse. I was told in no uncertain terms
that this was his “gaming mouse”, and he simply could
not replace it, as it had cost over $100 new.
I plugged it into my PC and ran it through its paces.
It certainly had many buttons, and they all worked as
expected, except the right button. It did indeed double-click with every single press.
The screws holding it all together were hidden under
more of those Teflon coated cushions, which I managed
to save.
Internally, the mouse looked like it was a nesting home
for a cat or other small pet. The internal optics for the
scroll wheel were buried under a soft blanket of pet hair,
which extended across most of the mainboard.
After I removed all that, I could test the microswitch on
the board, and sure enough, it was faulty. After removing
the small daughterboard, the mainboard came out, and I
removed the offending microswitch.
It was a fairly common part, even though it did have the
Logitech logo on the side, so I quickly found a replacement. It all worked fine once reassembled, and the young
gentleman was very happy.
I did mention the pet hair inside the mouse (shouldn’t
that be the other way around, mouse hair inside the cat!),
and he smiled and said the family cat often slept on his
desk, so that answered that question.
I have also repaired his monitor twice, once for a bad
tactile on/off switch and again when the mainboard
stopped working. Both were easy fixes, although I had to
buy 250 tactile switches in a nice neat little case; I will
soon be ordering more, as I replace more and more of
these switches.
Like Dave Thompson, my eyes are not so good nowadays, so soldering the 2.1 x 2.8mm switches required the
use of a desktop magnifier.
I also have a repair story involving Coca Cola and a JVC
65cm LED TV. I won’t bore you with the details; suffice
to say, it no longer worked.
The photo below shows what I found after checking the
power supply board and the T Con board. Coke always
makes a mess of electronics.
When these accidents happen, turn it off and get it to
a service person ASAP. Don’t ignore it just because the
TV (or whatever it is) still works. That’s what this teenage
customer did, and check out the resulting damage. After
I explained the fault and the time it may take to repair, I
got the feeling that this young fellow would be mowing
the lawn to pay Dad back for the cost of the repair.
It took a couple of hours to clean it up and get it working again. Rest assured that the offending teenager learned
a lesson and got Dad out of mowing for a while...
Damaged varistors in two microwave ovens
R. S., of Fig Tree Pocket, Qld has been busy fixing many
appliances, including two microwaves. Despite being
different models (both by Panasonic), they failed for the
same reason...
Both microwave ovens had intact mains fuses, but the
protective varistor across the mains on both microwave
ovens’ control/display boards were damaged. I think
this could be due to mains surges. This varistor is a
VDR10D511 10mm diameter, 511V varistor. There are also
protective capacitors on the mains supply input board.
The NN-SF574 oven (quite new) uses an inverter for
the control board supply with a Panasonic flyback control
IC and a high-frequency transformer. The varistor across
the mains is fed by a fine track marked PF1, which acts
as a fuse. This saved the board; replacing the track with
some fine wire and fitting a new varistor got the oven
going again.
A new control board is about $110, and a new oven
about $225. The NN-ST671 oven is an older design, with
The doubleclicking
mouse’s PCB,
shown at left,
had faulty
microswitches.
At right is a
section of the
power supply
board of a 65in
monitor. Some
corrosion can
be seen on the
connectors
from a soft
drink spillage.
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Australia's electronics magazine
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a small 50Hz transformer on the control board. Again,
the mains varistor is fed by a fine track, which I had to
replace along with the varistor. In this case, the varistor
was sleeved with a high-temperature fabric. Perhaps varistors have caught fire or exploded in the past.
I also repaired a Dome 24 wine cooler, Item No 900096.
Taking the back cover off showed it was a Peltier Effect
cooler with a large heatsink. There were two fans on the
outside to remove the outside heat, plus one on the inside
to distribute the cold air.
The constant current switching power supply for the
Peltier device had a blown fuse on the mains side. The supply uses a TL494 switching regulator driving two 13005
400V transistors connected in a totem-pole arrangement,
probably to increase the voltage rating.
Both 13005 transistors measured short circuit, as did
the STPS2045 dual schottky output rectifier (2 x 10A
45V). After replacing these, I put a light bulb across the
blown fuse and connected the mains. The bulb stayed on,
so there was still a problem.
I was surprised to find that two of the 1N4007 rectifiers
in the full-wave bridge were also shorted on the mains
input side. I am used to the large, sturdy rectifier bridges
used in microwave oven inverters which never fail; the
switching IGBT goes first.
Replacing the 1N4007s and the fuse got the cooler working again, with about 1.5V across the Peltier Effect device.
I did not measure the current. The big test will be when
summer comes, to see if the wine stays cool.
I also fixed a Kambrook K1780 steam iron. The series
capacitor in its power supply was a 560nF 250V DC
rated type that was down to about 430nF, so there was
not enough voltage to operate the 24V relay that connects the mains to the iron heating element. So the iron
would not heat.
I notice that the capacitor manufacturers derate the
voltage rating for AC, to about 60% of the DC voltage rating. For example, a 400V DC capacitor has an AC rating
of about 240V.
On that basis, the original 250V DC rated capacitor was
not adequate for the task. It seemed to have been chosen
for its small size, to fit in the space, rather than for a suitSC
able voltage rating.
The damaged VDR10D511 511V varistors taken from the
Panasonic microwave ovens.
siliconchip.com.au
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January 2022 95
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