|
Items Covered This Month
- Sony ST-E200
- Panasonic TC-2670S M15D chassis
- Panasonic TC-63A61 M16M chassis
- Philips 14PT132A/75R L7.01 chassis
- Sony KV-3400MAS SCC-C91C-A GP-2A chassis
|
My next door neighbour Leo likes to reinforce the Old Pals Act
(OPA) occasionally and get me to "look at" things that don't quite work right.
Leo's no slouch for a bloke of his advanced age and hearing, fancies himself as
a bit of an engineer and tends to "have a go".
Anyway, one Sunday morning while letting the cat in (at 7am!) -
and still in my pyjamas - he asked me to have a look at his Sony ST-E200 stereo
tuner. He had already removed the lid and pointing to some transistors
(subsequently identified as Q15 and Q16), informed me that the left channel
wasn't working because one of these emitter followers was crook.
Some hours later, when I was really awake, I humoured him by
looking at it in proper focus. This also meant opening the shop to get the
circuit - oh well; I hadn't anything else to do. Regretfully, this ruined my
plans to go to church and Mrs Serviceman was unimpressed with Leo's tuner in
pieces all over the kitchen table, especially with lamb roast on the menu.
Getting down to details, transistors Q15 and Q16 are
conventional muting transistors in parallel but one could cause this symptom. I
could confirm this by just disconnecting the collectors but I felt it would be
easier to use an audio probe and see if the audio was coming out of IC41 LA1835
(detector and decoder).
I confirmed this; audio was OK on each channel - on pin 21 (R
ch) and pin 22 (L ch). From here, each goes to one of two low pass-filters -
LPF42 (R ch) and LPF41 (L ch). Audio goes into each LPF on pin 2 and comes out
on pin 4. The audio was OK on the input and output of LPF42 (R ch) but was
absent on the output of LPF41.
The DC voltages were the same on each and I could see no harm
in patching pins 2 and 4 together on LPF41. I now had output from both channels
which meant that LPF41 was almost certainly open circuit.
Well, I could have given it back to him like that and I doubt
whether he would have heard the difference. But I knew he would have been
unhappy with a "bodgie" fix and would have interrogated me as to how I had fixed
it. So a replacement LPF41 went into the ordering process first thing Monday
morning.
Postscript: believe it or not, this part was not available in
Australia and had to be ordered from Singapore. It arrived the next day! The set
was soak tested and returned to its owner the next weekend.
Well, that really was an easy one.
(Editor's comment: whatever happened to the policy of changing
names to protect the guilty? I'm not too happy about this, especially the
comments about age. Life's pretty crook if you can't have a little service job
done without having it written up for the whole world to read about
it ;-)
A shame to work
The following Monday was a great morning. The sun was up in a
cloudless sky and even the kookaburras were telling everyone what a glorious day
it was and how good it felt to be alive.
I contemplated over my coffee that it was a shame to have to go
to work instead of going to the beach - especially as there wasn't really much
on. (At work I mean, not at the beach).
I felt that today would be a good time to sort out some old
stock and fix up some odd jobs left lying around. And so I turned to a couple of
Panasonic TV sets that had been put aside for a very long time and needed
investigating.
One was a 1990 TC-2670S M15D, which had been abandoned due to
an horrendous intermittent fault of no video when hot (it was invariably OK when
cold) and no sound.
The other was a 1992 TC-63A61 M16M, which I had been given a
couple of years ago with the picture tube (M63JUA07X) having no red. Its cathode
was completely stripped and I'd had no luck in obtaining a replacement because
63cm sets are no longer a popular size - it's now usually either 59cm or 68cm.
The other problem was that the tube is an FST (Flat Square Tube).
Well, today was the day I was going to resolve these and
hopefully other long standing problems.
The plan was to look at the older M15 and see if I could fix it
with information I had acquired since abandoning it. If that turned out to be
unsuccessful, my strategy was to try to fit the M15 picture tube into the later
M16 set.
The audio problem was easily fixed. There was no 18V at IC2301
pin 1 AN7158N, due to R827 (0.22Ω) being open circuit.
It took longer to fix the picture failure when hot. I started
with the usual suspects, namely R525 (100kΩ - check this out of circuit or waste a
lot of time) and Q601 (UN1111, DTA114EA), but these were OK. The latter, by the
way, can be replaced with a general purpose PNP transistor such as a BC558, with
10kΩ in the base
and 10kΩ from
base to emitter.
In the end, the fault turned out to be just faulty joints and
some corrosion. The picture wasn't bad but the 12-year old set was corroded and
dirty and very much the worse for wear.
Finally, I made a decision - I would scrap this set (with a
good working chassis) for parts and transplant the tube to the later model
set.
Removing the tube
Removing the tube was relatively easy, except for the time
needed to remove the case. The tube is so large and heavy and the cabinet is
very light and tends to move. Also, there is very little room for one's fingers
to get a grip around the rimband. I put a plastic lunchbox underneath to take
the weight of the tube as it came away from the four studs and the case
supports. I could then rearrange my grip and get a better purchase.
I made the mistake of trying to put the replacement tube in the
M16 cabinet face down instead of leaving it vertical (the empty cabinet was just
too flimsy and kept moving). The result was that although I fitted the tube in,
it was 12mm out but stuck fast. When I eventually moved it into the correct
position, it fell heavily those last 12mm onto its face but a quick inspection
later on indicated that everything was probably OK.
I was going to replace the deflection yoke but the one already
on the tube looked identical to the original. Not only that but the plug fitted
straight into the DY position. Also, the wire colours matched. I refitted the
chassis and after a final check, switched the set on.
It tried to come on but then stuck in standby. What could I
have done wrong? Well, lots as it turned out.
I removed D560 and switched on. Smoke rose out of the power
supply board (D). It took a couple of hours to work out what I had done. As it
turned out, the M15D deflection yoke (Part No: TLY15459F) differs from the M16M
yoke (Part No: TLY15493F). Not only that, the DY plug is wired differently
despite the fact that the wire colours are the same.
As a result, high-voltage horizontal pulses were injected into
the output of the vertical IC (IC452, LA7838), destroying it and causing R570
and R451 to overheat and smoke. At the same time, additional current flowing
through R578 in series with R570 caused Q557 to switch on and so the protection
circuit was switched on.
But this was only the beginning. It took two ICs to find out
that D460 (MA4360M), a 36V zener, was also short circuit.
Finally, after it was all fixed and the set was switched on,
there was only a blurred smudge on the screen, a noise and the smell of burning.
This turned out to be a fracture suddenly appearing in the tube neck under the
yoke, with arcing everywhere. The tube was kaput!
I had waited a couple of years to replace this tube and I was
now determined to fix the set. I tried all my colleagues (again) and was lucky
to find one who had just scrapped an M15LW chassis, so I took the tube back and
fitted it into the M16M, this time with a lot more care.
I was also careful while transplanting the deflection yoke and
in fact everything associated with the tube. In the process, I removed all the
old parts, including the chassis strap and degaussing coils, and put them on a
shelf above the set, behind some aerosol cans.
The new tube worked well but when I reached up for a can of CRC
2-26, the old chassis strap got caught and fell straight onto the M16M chassis
beneath. Unfortunately, it was switched on at the time and there was a small
spark as I dashed for the main power switch.
After removing the offending chassis strap, I tried to work out
what damage had been caused. The strap was nearly half a metre long and could
have touched the righthand loudspeaker as well as the high voltage power
supply.
On switch on, I confirmed there was now no audio and R819
(0.47Ω) in the
25V rail was open circuit. Replacing it caused the new one to smoke very quickly
so I replaced the sound output IC (IC2301 MC13500T2) but there was still no
sound and R819 was still getting hot.
Next, I measured the rail and found that it was only 14V when
it should have been 25V. However, when I desoldered pin 9 of the audio IC, the
voltage rose to its correct value.
I had fitted a TA8200AM audio IC instead of the MC13500T2 which
should have been OK. So was there any modification required? I spent a lot of
time on this red herring before I woke up that the lefthand loudspeaker voice
coil was short circuit - not the righthand one, as I had suspected.
Unfortunately, the speaker is a custom 8Ω 10W oval type, so it will
be difficult to get an exact match. In the meantime, I've substituted a similar
unit which fitted after a session with the electric drill.
And what is the moral of this story? If it starts out to be a
beautiful day and if the planned exercise looks easy, it can still end up like
the pits.
Philips portable
I don't get many portable TV sets these days, as they are so
cheap to buy now. Occasionally, they do arrive and when a 1997 Philips
14PT132A/75R (L7.01 A chassis) came in with no audio, I assumed it would be a
simple fault. I mean, a TV set with no audio - how hard can that be? There was
no audio from the loudspeakers or earphone socket on either TV or AV input.
This particular set also had Teletext and "SMART" controls
which give a selection of preset Picture and Sound positions to enhance the type
of program selected.
To get into the SDAM (Service Default Alignment Mode), I needed
to short M24 and M25 and switch on. However, there were no error codes. Standby
leaves this mode.
I measured loudspeaker continuity right back to pins 6 and 8 of
IC 7120, a TDA7065B 3W audio amplifier. I measured 16V (Vcc) to pin 2 and an
audio probe showed that audio was getting to the pin 3 input. That only left pin
5, the DC volume control - it had no voltage on it at all.
With the set switched on, I connected my old analog multimeter
(on the x 1 resistance range) between pins 5 and 4 (chassis). Suddenly the room
was filled with sound.
The DC volume is controlled by pin 2 of the microprocessor
(IC7601, SAA5290ZP/072) and is connected by R3630, a 10kΩ SMD resistor. However, there are 11
other components hanging off this line, mostly diodes, capacitors and
resistors.
Using a digital multimeter, I measured the impedance to chassis
and it read over 3MΩ. So no short circuit, I thought. That left 11 components to check apart
from the two ICs - a piece of cake.
First, I changed the audio output IC (it has only 9 pins), in
case an internal diode protection circuit was dragging the voltage down. It
wasn't.
Next, I measured 1V on pin 2 of IC7601 but nothing on the other
side of R3630. The voltage on pin 2 varied from 0-3.3V, depending on the volume
setting. I checked R3603 from the 5V rail to pin 2 as 8.2kΩ and R3630 was correct at
10kΩ.
I then disconnected the three diode clamps on the line and
replaced the two electros. I also measured the remaining resistors - everything
checked out OK. So where was the voltage being held down?
The remaining components were all surface mount devices (SMD).
They are not only very small but are also glued to the PC board, making them
difficult to remove. I tried heating and freezing them to see if any responded
but nothing showed up.
Finally, I desoldered pin 5 of IC7120 from the board and
soldered this pin (only) to a jumper lead connected directly to pin 2 of the
microprocessor. Finally, I had voltage and sound which was now controllable.
That led me to my chief suspect - SMD capacitor C2121
(0.22μF). Even
though I had checked the resistance of this capacitor several times in circuit,
I now found after removing it that it measured only 586Ω. This was definitely the culprit but
why didn't it measure low before?
One possibility is that this device might have been
intermittent and only showed its true - and permanent - leakage after the stress
of being removed.
Or was I deceived by the meter? Digital meters are
fundamentally more accurate and have both advantages and disadvantages compared
to analog types. One advantage is that they can often accurately measure
component values in circuit, since the voltage they apply is too low to switch
on active components such as diodes and transistors.
On the other hand, the measuring voltage from a digital meter
is too low to place the component being checked under stress. Older analog
meters use 9V or 22V batteries and can detect leakage better because components
are being checked under more realistic working conditions.
A big Sony
An 80cm Sony TV monitor was dropped in for repair. I say
"dropped" but I don't mean it literally - this set weighs in at 74kg and
something would certainly have broken if it had really been dropped.
I had never previously seen this model - a KV-3400MAS
SCC-C91C-A, using a GP-2A chassis. It was owned by a recording studio and
someone had obviously had a look at it, as some boards were loose inside and
some metal covers had been removed. All I was told was that it was dead and they
asked if I could "please, please fix it ASAP". Fortunately, a service manual was
supplied with the set.
The section where the covers had been removed was the power
supply (F1) and I could see that all the electros had been replaced recently by
someone who knew what he was doing; the work was clean and the soldering good.
However, after a few resistance checks, I confirmed that PS653, a 2.7A IC link
fuse that looks like a two-legged transistor, was open circuit. This is the
source of the 15V B line going to CNO20 (pin 1) on the D Deflection Board and on
to IC503 (STR90120), a large switchable 12V IC regulator.
With all the modules plugged back in, the symptoms at this
stage were that the set would try to come on, with red LED D41 on the front
indicator panel H coming on for a few seconds; otherwise the set was dead. There
was no sign of distress anywhere else, which I thought might have caused the
blown fuse.
My approach now was to follow the two rails, looking for
something that was drawing too much current. I disconnected the modules one at a
time as I progressed and when I disconnected the B Chroma Decoder board, the set
fired.
Elated, I followed the 12V everywhere on the B board,
desoldering devices everywhere in an attempt to find out what was causing the
set to die. Finally, I reached the Comb Decoder IC (1310) and disconnected the
9V rail (via Q1360 from the 12V rail) to pin 1. Once again the set fired.
However, after spending a lot of time up and down this path, desoldering and
resoldering everything, I finally realised that the fault was intermittent and
wasn't due to anything on this board.
It took a while to work out what was going on. Something was
activating the protection circuit and switching the set to standby. Because of
the PS653 fuse failure, I had assumed that it was a short circuit on the 12V or
15V rail that was responsible but that turned out to be a red herring.
I established that there was 135V on the horizontal output
transistor (Q804) collector which was correct but the 135V on the horizontal
drive transistor (Q805) was not right. Instead, it meant that this transistor
was cut off and I found that it had no horizontal pulses coming in from the
jungle IC (IC501, TEA2028B). However, the oscilloscope showed me it was trying
to come on momentarily.
Among others, the circuit that interested me was the safety
circuit involving Q806 and Q807 from pin 4 of the horizontal output transformer
to pin 28 of IC501. Transistor Q806 detects the current flowing through R843 to
the horizontal output stage and if it's excessive, applies voltage through
inverter Q807 and switches off the oscillator in the jungle IC.
It was here that I found the circuit in the service manual was
quite different from the one in the set. In particular, R842 turned out to be a
zener diode but it checked out OK.
The safety circuit wasn't being activated, the collector of
Q806 was correct at 0V and Q807 seemed correct too. Desoldering pin 28 of IC501
restored the picture. So what was happening between that and the collector of
Q807? I traced the circuit and found it went near a mounting screw. Careful
examination revealed a hairline fracture across seven PC tracks and it was this
that was causing the intermittent fault.
The fracture was extremely fine and the tracks extremely
narrow, so it took a lot of effort to solder tiny links across them. I was just
completing this when I had an attack of stupidity. I had been using solderwick
on and off on all the work I had been doing and when not using it, I had just
placed it on top of the power supply which still didn't have its metal covers
replaced.
When I had finished, I tidied up and removed the tools and
reassembled the boards - but I hadn't noticed the solderwick.
I switched the set on and there was an almighty bang from the
power supply. I immediately switched off. It was fairly obvious the copper wick
had shorted out the power supply but what was the extent of the damage?
The violence of the short had melted two welts on the big
aluminium heatsink. I removed the power supply and checked it all carefully -
but amazingly could not find any fault. The copper braid had shorted the live
side of the chopper transformer to the chassis side and the main circuit breaker
had saved the day.
I reassembled everything with much greater care and switched
on. This time the set came on properly. I connected video and audio and the
picture and sound were good.
So that was it - but I was lucky with the solder wick
incident.