PC Boardsfor most Silicon Chip (plus EA
& ETI) projects can be obtained from RCS Radio, Sydney.
Phone (02)
9738 0330. Fax (02) 9738 0334. Email sales@rcsradio.com.au or visit
www.rcsradio.com.au
Low Ohms Tester for DMMs, February 1988:
the 10kΩ feedback resistor between pins 6 and 2 of IC1 is incorrectly shown
on the wiring diagram (Fig.2) as 1kΩ.
Protector Car Burglar Alarm, February 1988:
in some projects, the 4027 (IC2) has been damaged by voltage transients from
the ignition cutout relay. To solve this problem, delete the link connecting the
emitters of Q7, Q8 and Q9 to the earth track (ie, delete the link immediately to
the left of Relay 1 - see Fig.2, p.22).
A length of
insulated hookup wire should then be run from the now vacant pad adjacent to Q8
directly to the Ground input on the PCB terminal block on the left hand side of
the board.
Remote Switch for Car Alarms, March 1988:
the inductor marked L2 in the receiver should have an F29 slug, not F16 as
specified.
Remote Switch for Car Alarms, March 1988: a small inductor should be inserted between the base of Q2 and the negative
side of the 2.2μF capacitor in the receiver circuit. This is to prevent RF
energy from reaching IC1a and thus desensitising the circuit.
The
inductor can be made by winding eight turns of 0.63mm enamelled copper wire on a
3.2mm former (ie, a 1/8th-inch drill bit). It can then be installed directly on
the PC board in place of an existing wire link. Note that the 2.2μF capacitor is
shown with reversed polarity on the overlay diagram and should be installed the
other way round.
Finally,
the 100k resistor connected to the base of Q2 should be reduced to 47k to
increase the damping across L2.
This
project was also the subject of a "Kit Clinic" article in the January 1989
issue.
UHF Remote Switch (March 1988) & UHF
Remote Chime/Doorbell (August 1988):
some readers have reported difficulties
with these projects. Here’s how to solve the problems:
First, readers
should note the errata above for the UHF Remote Switch receiver (March 1988).
These changes were all incorporated into the UHF Remote Chime/Doorbell (August
1988).
The kits we
inspected failed to work because of incorrect component types and values. The
following comments apply to both projects:
Transmitter: low-voltage miniature
ceramic capacitors must be used where specified. Keep their leads short by
pushing them all the way down onto the PCB. Do not use the larger 1kV ceramic
capacitors. Their stray capacitance will upset the tuned frequency and can
result in a transmitter that continues oscillating after the power switch has
been released. Result - a flat battery.
Similarly, the
0.1μF capacitor must be a miniature polyester type (do not use a metallised
polyester type). The trimmer capacitor must be a 2-6pF type as specified - you
will not be able to correctly set the transmitter frequency with other values.
Receiver: the four .001μF capacitors
used in the front end must all be ceramic types as specified. Do not use
metallised polyester (greencap) types - they don’t operate well at 304MHz. L3
was also found to be incorrect. It must be a 3.3uH inductor (a 3.3mH inductor
will seriously degrade the sensitivity of the receiver).
Finally,
the PCB patterns were inadvertently omitted from the wiring diagrams for the
Remote Chime/Doorbell (p.59, August 1988). The diagrams are reprinted on page
103 of the September 1988 issue.
Optical Tachometer, May 1988:
the 10μF
electrolytic capacitor connected to the cathode of photodiode ID1 is shown
reversed connected on the wiring diagram on page 20. The circuit on page 19 is
correct.
High Energy Ignition System, May & June
1988 (and May 1990):
a letter concerning this electronic ignition on page 91
of the March 1993 issue suggests the use of a plastic case with a metal lid, to
eliminate problems with punch-through of the transistor insulating washer. We
strongly recommend against this approach as the high voltage on the case lid
could give a nasty shock to an unwary user.
To help
prevent arcing and punch-through, we recommend that the holes in the case for
the TO-3 transistor be lightly chamfered to remove any swarf. The use of two
insulating washers is also a good approach.
High Energy Ignition System, May
& June 1988 (and May 1990):
we recommend against using sport ignition
coils such as the commonly available “GT40”. These coils draw more current than
the original vehicle’s coil and may seriously overheat.
Automatic Light Controller, June
1988:
there are two errors on the circuit diagram on page 57; pins 12 and 13
of IC2c are shown transposed, as are pins 4 and 6 of IC1. The wiring diagram on
page 59 is correct.
Also the
text in paragraph two, column three, page 58 should state “This low signal is
then inverted by IC2d and the resulting high applied to pin 12 of IC2c via D10
and R7”.
RF Sniffer Probe & Preamplifier,
June 1988:
the circuit diagram for the RF Sniffer Probe published in the June
1988 issue was for an initial prototype, rather than for the final version which
was shown in the coded photograph. The diagram on page 80 of the September 1988
issue shows the correct version, the main differences being the connections for
the 470Ω base bias resistors on transistor stages Q1, Q2 and Q3.
The supply feedpoint was also shown incorrectly - it should go to the
midpoint of the two 10Ω resistors. The coded photograph published on page 73 of
the June 1988 issue is correct as are other constructional details.
Studio 200 Stereo Control Unit, June 1988:
the following parts should be added to the parts list: 2 x 100μF 16VW PC
electrolytics, 2 x 0.1μF metallised polyester, 1 x .01μF 250VAC (Wima MP3 or
Philips MKT-P 2222 330 40103).
Studio 200 Stereo Control Unit, June 1988:
experience with the control unit when teamed with a number of power
amplifiers has shown that the combination can oscillate supersonically when the
Treble control is at maximum and the Volume control is at high settings. While
these are abnormal control settings, if oscillation is allowed to persist it may
damage the power amplifier or the speakers.
To prevent the
condition occurring, we suggest that an additional 270pF capacitor be connected
across the 4.7k feedback resistor for IC2 in each channel.
In addition, a 560pF
capacitor should be connected across the volume control potentiometer; ie, one
560pF capacitor across VR1a and one across VR1b.
Studio 200 Stereo Control Unit, June, July
1988:
we have had a report of overheating of the output transistors in the
headphone driver amplifiers. This is possibly caused by mismatch between diodes
D1 and D2 and the transistors Q1 and Q2.
We
therefore recommend that D1 and D2 in both channels be replaced with 1N914s or
1N4148s.
Studio 200 Stereo Control Unit, June, July
1988:
in spite of the notes published regarding D1 and D2, a number of
constructors have still experienced overheating problems with Q1 and Q2 in the
headphone driver amplifiers.
To cure
this problem, 33Ω emitter resistors should be installed for Q1 and Q2. To do
this, disconnect the emitters of Q1 and Q2 from the PCB and wire the
33Ω resistors in series, between the PCB and the free emitter leads. This will
slightly reduce the available headphone drive level. If this is critical, reduce
the 82Ω resistor to 47Ω .
Remote/Alert Doorbell, August 1988:
when
setting the transmitter frequency for Q1, do not connect pin 15 of IC1 to the
+12V supply. This can damage IC1. Instead, disconnect the 47k resistor from pin
15 and connect it instead to the +12V supply to make the transmitter run
continuously. (See also the notes
over the page.)
Universal Power
Supply Board, August 1988:
the 1000μF capacitor in Fig.8 (parts layout) is
shown with reversed polarity. (11/04)
Hands-Free Speakerphone, September 1988:
the 1μf capacitor shown connected to pin 17 on the circuit diagram of page
17 is the wrong way around. The wiring diagram on page 19 is correct.
The text on page
19 concerning the “initial circuit checks” has an error. The external 25 to
50-volt supply should be connected via a 560Ω resistor to board inputs 1 & 6,
not 1 & 3.
Fish Bite Detector, September 1988:
all
the diodes are shown reversed on the wiring diagram. The circuit diagram is
correct.
Switchmode Battery Charger, September 1988:
pin 11 of IC1 should be shown earthed on the circuit diagram.
FM Stereo Transmitter, October 1988:
the
0.01μF filter capacitor connected to pin 12 of the IC should be 0.001μF. With
the 0.01μF in place the transmitter will not work in stereo.
Poor Man’s Plasma Display, November 1988:
the Veroboard wiring diagram on page 44 contains an error in the wiring to
the 555. Pin 3 is shown connected to the positive supply line. The copper strip
between the 1k resistor and short supply link should be cut.
120W Public Address Amplifier, December
1988: the switch contacts 1 and 2 associated with the 6.5mm jack socket (top
lefthand corner of the circuit) should be shown normally open, not normally
closed. The wiring diagram on page 45 of the January 1989 issue is correct.