Items Covered This Month
- Kikusui COS5060TM 60MHz delay oscilloscope
- Technics RS-1500US professional reel to reel tape recorder
- Sharp CX68GS TV set
- Philips CH685 TV set (KL9A-3 chassis)
- Superloos – a close encounter of the toilet kind
- Grundig Megatron M82-115/9 IDTV/P+P TV set (CUC1882 chassis)
- Philips 32FL2881/75R TV set (FL2-G chassis)
- Panasonic TX-51P800H (GP1 VP chassis)
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I think I’m over servicing oscilloscopes. The only thing they
seem to have in common with TVs is the CRT and even then the voltages are all
completely different and difficult to measure.
Basically, you need a digital voltmeter that can read from
-3000V to over +12,000V. Unfortunately, using a 30kV probe with an analog meter
is rather difficult – especially when it comes to making contact with a tiny,
inaccessible component without shorting anything.
Anyway, I had to fix a Kikusui COS5060TM 60MHz delay
oscilloscope that had excessive uncontrollable trace brightness. I don’t know
its age (I guess about 1983) but the look and feel of this CRO is very similar
to that of the LG/Goldstar ones I have written about recently. It even uses a
very similar Toshiba 150CTB31 CRT (16W).
However, unlike the others, there are no voltages or control
descriptions written on the PC boards, the access is much worse and there is no
circuit diagram in the instruction manual.
Once I began looking inside, it was hard to know where to
begin. In the end, I decided to start my attack with a soldering iron and
resoldered as many dry joints as I could find, especially in and around the
power supply and EHT sections. I found one "doozy" of a classic dry joint to the
CRT filaments but nothing that made any significant difference to the fault at
hand. All the other controls appeared to work and the intensity control was
having a slight effect, mainly due to the size of the sweep and focus which I
put down to "blooming" from the excessive beam current.
Next, I tried to figure out where the CRT bias control was but
was unable to be sure. There are three largish trimpots next to the CRT
connection plug which I marked before seeing what effect they had. However, they
seemed only to have an impression on the trace focus.
By now, I desperately needed a service manual and so I got onto
the web and started looking. Google revealed no private copies and virtually no
information at all but I did discover that the Australian agent for Kikusui was
Emona Enterprises. As a result, I contacted their spare parts division and
enquired about purchasing a service manual.
A few days later, I was informed that the complete service
manual was available for $150 plus GST (three weeks ex-Japan). Unfortunately,
this price was out of my league but a very obliging young lady at Emona managed
to organise a deal for me that was acceptable. She could supply a few relevant
photocopied pages for $25. I jumped at this generous offer and in due course not
only received the complete circuit diagram but also three BAV21 diodes that
Emona’s technical section thought might be the cause of my problem (CR835, CR837
and CR838 in the G1 circuit to the CRT).
Well, that was service with a smile! I removed and checked the
three diodes but unfortunately could only find CR835 to be slightly leaky.
Replacing all three made absolutely no difference to the symptoms. I now knew
that the CRT BIAS control was RV821 but it too made no difference to the
fault.
Another disappointment was the lack of voltages marked on the
circuit, although I managed to confirm the few that were marked as being
correct. Using a high-voltage probe, the cathode measured -1.74kV, the first
grid -1.76kV to -1.77kV (depending on the intensity control) and second grid
(P1) -1.16kV (Focus). The third grid (Geom/Accel) was +45V and the fourth grid
(Astig) was +63V, which was roughly what I expected.
G1 with respect to the cathode was varying between -20V and
-30V but when I connected a DVM between these elements, the voltage range was
different, this time varying from -8V to -20V (minimum to maximum intensity
respectively). Similarly, the second grid to cathode measured 580V with the
probe and only 190V with the meter. I’m not sure why these discrepancies
occurred but I suspect that the DVM was dragging the voltages down.
Unfortunately, I couldn’t measure the EHT as access was too
difficult, the probe being wedged hard between the CRT and the front control
panel. Any attempt I made caused severe arcing and threatened to destroy the
circuits!
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Using another oscilloscope, I could see the "Unblocking Signal"
coming into the CRT control DC regeneration circuit. This varied with the
front-panel controls but I had no definitive figures to work with. At this
point, I noticed two circuits that were very similar, one for intensity and the
other for focus, so I compared their voltages. It turned out that the focus
control voltages were much higher than those for the intensity control circuit
(95V compared to 45V) but was this significant?
Because the BAV21 diodes were obviously recognised as
troublesome components by Emona, I decided to check all such similar diodes in
both of these control circuits. To do this, I unsoldered one end of each diode
and measured its leakage with x100kΩ ohmmeter but I couldn’t find any that were
faulty. Similarly, I checked all resistors over 47kΩ and even replaced C846,
C847 and C848 (1nF 6kV) in case they were leaky but I was getting nowhere.
By now, I was seriously considering abandoning this project
when a colleague volunteered to look it over for me. It took him only an hour to
find the culprit which turned out to be CR836, a BAV21 from the wiper of the CRT
Bias control (RV821) which I had already checked. It was indeed leaky but how
did I miss it? I could swear I had measured it to be OK out of circuit but
obviously I had missed it (I must be getting old). Anyway, this fixed the fault
completely.
I must admit that I am now highly suspicious of all BAV21
diodes and will in future always measure them completely out of circuit as they
never go dead short. Instead, they always seem to go high resistance!
Interestingly, I went back in afterwards to see what voltage
differences it had made and found that the only change was to G1. This now
varied from -62V (minimum intensity) to
-43V (maximum intensity).
Ironically, in the course of measuring these voltages, some
small sparks were produced as the meter probe touched the solder pads and
suddenly the fault was back again. This time, it was CR835 that was
faulty.
A real recorder
An enterprising client of mine purchased an old but beautiful
Technics RS-1500US professional reel-to-reel tape recorder. In fact, he bought
this "Isolated Loop", 3-motor, 3-speed (15, 7½ , 3¾ ips), direct quartz
locked-drive, 4-head tape deck along with 40 10½-inch reels of tapes. In its
day, it was probably one of the finest tape recorders made and he paid for it
outright by selling some of the tapes on eBay.
However, he struck a catch – the deck was faulty! None of the
"turbo-touch" controls were working!
Unfortunately, access to the circuits in this machine is very
difficult. Those Japanese must have very small hands, because you almost need to
perform keyhole surgery when fixing this deck.
When I finally managed to remove the power supply and main
control circuit, I started by checking the main power rails (21.4V, 20V, 15V and
5V). These were all spot on so I moved on to the six microswitches (or remote
control), which controlled the input NAND gates of seven logic ICs via 12
diodes. These in turn control the motors, plus an additional timer circuit.
I soon found that the STOP input rail (D3, D6, D9 & D19)
was perpetually held low, so I checked these diodes as well as D15, D16 (from
the timer), D17 and D18 plus TR8, TR24 and TR25 but they were all OK.
In fact, I didn’t get anywhere until I checked out IC7
(M53200P), especially pin 11 (LO) which is controlled by pins 12 & 13 (HI).
This in turn is controlled by TR10 (2SC828) and D26 which was switched off.
Both TR9 and TR10 measured OK, which just left C17 (4.7μF 10V)
on TR9’s collector. This was short circuit and replacing it fixed up all the
functions.
Zapped Sharp
Mr Marsden brought in his Sharp CX68GS TV set that had been
killed during a storm – or so he thought as he wasn’t actually there when it
happened. Looking inside, I quickly found that R706 (1.8 7W) was open circuit
and that chopper transistor Q703 (2SC4429) had shorted.
With a switchmode power supply like this, you have to check
everything in order for it not to blow again – especially after a cataclysmic
event like a power surge or lightning strike. Subsequent checks revealed that
C715 (0.01μF), R711 (47Ω 0.5W), Q702 (2SC3807) and C716 (2200pF 2kV), the latter
sporting a black burnt spot (and probably the main culprit), were all in various
stages of destruction. I replaced them all with identical components, some of
which had to be ordered in.
I switched it on and BANG – the front face of the chopper
transistor blew off completely. Oh dear! I installed a new chopper transistor
and replaced Q702 (2SC3807), 5A fuse F701, IC703 (SE120N) and the optocoupler
(IC702), before rechecking everything I had already done. That done, I gingerly
switched the set on again and . . . CRACK! – it all blew up again (and the parts
ain’t cheap).
This time, an even closer recheck of everything revealed that
only transistors Q703 and Q702 and the fuse were damaged. The 2SC4429 is rated
at 1100V, 8A & 60W and the 2SC3807 at 30V, 2A. It seemed obvious to me that
the chopper was failing and blowing its driver, so I decided to install a BU508A
(rated at 1500V, 8A, 125W) instead of the 2SC4429.
This time, when I switched the set on, it came on perfectly
with all functions working.
At that point, I decided that I’d had enough of the 2SC4429s
supplied to us and sent back all the other unused ones I had ordered. Frankly, I
think that they were underrated counterfeit copies of the original. In fact, if
you open up one of these devices, the "chip" is much smaller than you would
expect for a 60W device. Unfortunately, there are a few re-labelled counterfeit
power transistors around these days.
After soak testing the set for a week, it went back to Mr
Marsden. However, the very next day, he phoned and reported that it had died
again. I couldn’t believe it!
Back came the set and I was expecting the same problem as
before. However, I was relieved to find that it was only R705, the other sister
1.8 7W surge resistor from the bridge rectifier. That was some months ago and
so far, so good.
The humming Philips
I’m still getting in ancient Philips TVs which their owners are
reluctant to upgrade and the faults are becoming more weird and interesting.
Recently, a 1986 CH685 KL9A-3 chassis came in, its owner
complaining of a loud persistent hum in the sound. I thought at the time it
would be a doddle to fix but it turned out to be rather tricky.
In greater detail, the problem was 50Hz hum which was causing
the sound to "quaver" at low volume. This set has a separate audio output
amplifier board with its own power supply, so I checked the 33.5V and 15V rails
for ripple and tried unplugging the input to the amplifier module to confirm
that the problem was elsewhere.
I then backtracked towards the tuner, unplugging leads as I
went, and noticed that the hum would vary as I moved the modules and their
wiring harnesses. Aha, I thought, dry joints on these boards might be the answer
but there were none to be found.
It was then I noticed that the hum was varying with picture
content and that the objects on the screen were very bright and "contrasty". As
a result, I checked the aquadag screening from the CRT to the neck board and
found that uncoupling it removed the hum. I then clipped a jumper in its place
and earthed it to the chassis.
The sound was now back to normal and I spent a long, long time
trying to find out why this was so. This involved following the earthing to the
aquadag back to the EHT and tripler sections but I couldn’t find out what was
wrong. This wretched set was going to fight me all the way.
I then began to notice that the most sensitive board to
movement was the 5-pin DIN input module which also had a small 15V power supply
and an analog switching IC (IC7031, HEF4066). And although I couldn’t find
anything obviously wrong with it, I did notice that unplugging the TV input into
the IC also removed the hum. I checked the switching voltage from the control
panel TV/VCR switch and noticed that unplugging it also eliminated the hum.
I now felt that the problem was around this area and so ran DC
checks all around transistor Q7025 and IC7031. This turned to be quite fruitful
as it quickly revealed that R3040 (22k) to the base of this switching
transistor was open circuit, leaving the transistor permanently switched on. And
that in turn meant that two analog switches from the external DIN socket were
connected permanently.
So why did this resistor cause so much strife? My theory is
that when it went open circuit, it meant that the switching line cable probably
became inductive and was picking up 50Hz buzz from the CRT and passing that
through into the audio output stages. But then again . . .
Flushed with success
I was asked by a friend just recently if I could give him a
hand with some toilets! Apparently, he wanted me to help flush out some
problems!
Now these wasn’t just any toilets. Instead, they were the
public toilets for a very expensive architect-designed restaurant and were the
latest when it came to fantastic features.
For example, the men’s latrine has an automatic flush and the
glass hand "basin" was also completely automatic. The water was controlled by a
sensor and piped around the face mirror and flowed onto a piece of glass before
exiting into a trough. You washed your hands in the water from the mirror
faucet.
But it didn’t end there. The toilets had clear glass cubicles
and when you went inside, a sensor would make them go opaque for 90 seconds or
until the sensor no longer detected any movement. There is, fortunately a
fail-safe feature – in the event of a power failure, the glass remains opaque.
Flushing was via a touch sensitive area on the glass wall. All this for a mere
$100,000 and that was just for the glass panels.
Well, with all these high-tech features, things were bound to
go wrong and they did!
What no-one had envisaged was that apparently some young women
liked to go into the toilet and take a nap! The problem was that after 90
seconds the glass would clear and they were visible in all their glory!
This was, of course, the down-side. The upside is that if
someone is drunk or ill, someone will see their plight and presumably call for
help. Anyway we had to go back and see what could be done to make the sensor
more sensitive.
The infrared proximity sensors are mounted in the roof, one
above each cubicle. Initially, my friend specified very sensitive
small-footprint sensors but it was felt by management that a wide footprint
would better, even if it meant a reduction in sensitivity. Unfortunately, this
led to the current problem but I guess that’s all part and parcel of the
teething problems involved with new technology.
Anyway, we replaced each sensor so that the smallest movement
of someone sitting on the toilet would trigger it. We also realigned the sensor
with the crosshairs towards the front of the seat where one’s head would
normally be. The theory is that if the occupant falls asleep, their head will
remain in the sensor’s footprint and slight movements will continue to trigger
it.
This we hope will be sufficient, otherwise we may have to
contemplate fitting a horizontal infrared LED, mirror and receiver from behind
the occupant.
So there you have it – a fully automatic, timed and hygienic
ergonomic superloo. High-tech is everywhere!
Grumpy Grundig
I was recently asked to look at a 1996 Grundig Megatron
M82-115/9 IDTV/P+P employing a CUC1882 chassis. Initially, I thought the
"Megatron" bit referred to the extra-long model number but I later discovered
that it refers to almost every aspect of this luxury TV, which is modestly
described in the sales brochure as a "Megavision Monolith". And in case you’re
wondering, the set came with a $A9000 price tag – and that was back in 1996.
The client complained that the convergence was poor and that
there were lines across the picture. He also clearly implied that there wasn’t
really much wrong with it that a competent technician and $75 couldn’t fix!
Yeah, right!
When I opened up the 76cm set and examined it on the bench, I
did notice that the convergence was out but the only controls were the purity
and static convergence rings around the neck of the Toshiba A76KJJ96X98 picture
tube. Fortunately, it didn’t take long to fix the convergence problem, though I
have to say the 2mm dynamic convergence errors didn’t impress me in a $9000
television with no additional correction.
The main symptom, though, was still there and that was the
diagonal patterning which, when the colour saturation was increased, became
magenta stripes. I then noticed that the Picture-in-Picture didn’t have these
stripes but the picture was ghosting. This combination of errors was a dead
giveaway for a fault in the digital comb filter in the "features box".
I couldn’t continue without the aid of a circuit diagram so I
contacted Grundig, who were extremely helpful, and discovered that an exchange
features box was $385 trade. However, their technical support went beyond the
call of duty and told me to look out for a crack in the tripler and to change
all 26 electrolytic capacitors inside the features box (upgrading their values
to 220μF 35V 105°C).
This advice was spot on. There was a crack on the concealed
underside of the tripler (where the internal focus resistor is) and indeed all
the electrolytic capacitors inside the features box were shot.
Replacing all these items fixed the problem – but at a lot more
than $75. Ironically, after fitting the new tripler, the set would try to start
but would stop almost immediately. This was due to your truly forgetting to
reinsert a plug immediately under the tripler. It took a long time to find and
correct this as it was so well concealed.
One very impressive feature of this set was the amazing menu
system, which was a complete in-depth instruction book available in multiple
languages, plus a series of complex test cards and a service menu that can
perform service adjustments after dialling up the service code of 8500.
The beautiful Philips
I had another beautiful TV come in this week and I found it
hard to believe how technically advanced it was for a 1993 model. This was a
Philips 32FL2881/75R employing an FL2-G chassis and boasting a 16 x 9
widescreen, progressive scan, Dolby surround sound, picture-in-picture and 100Hz
scanning, to mention just a few of its features. Of course, all these features
came at a price, the set costing around $6000 11 years ago.
This particular set was dead and pulsating, so the first step
was to check out the HT rail. This involved shorting out the base and emitter
terminals of the line output transistor and hanging some 240V light globes (200W
total) across the collector. When I switched it on, the power supply had no
trouble delivering 140V into this 200W "dummy" load.
This was screaming at me "flyback transformer", except that
when I removed the shorting jumper and disconnected the horizontal deflection
coils, the B+ was restored and the set stopped pulsating. In the end, I decided
that the line output transformer was still the most likely culprit as there was
no discernible EHT.
This turned out to be correct. After fitting a replacement and
aligning the double focus control, the picture and sound were once again
excellent.
Where will it end?
With modern TVs, it is not unusual to include a set of software
convergence and other adjustments for both PAL and other systems as well.
However, we recently came across a convergence problem that initially had us
stumped.
The set concerned was a Panasonic TX-51P800H (GP1 VP chassis)
that came in with a faulty green tube with a focus problem. After replacing the
picture tube and doing all the alignment adjustments, everything was looking
great apart from a bizarre fault: the convergence was out only in the tuning
menu and the double window option.
At first we thought that this was due to a faulty EEPROM or
digital board. We were about to order and replace these items when the Panasonic
Technical Officer whispered in our ears.
Because we didn’t have the service manual, we could be forgiven
for not realising that the Tuning Mode Search Menu switched the set to
Progressive Scan and there is a separate set of convergence controls for this.
Similarly, the double window has its own set of controls too.
To fix this, you get into the "Service Adjustment Mode", select convergence,
and then select the mode (system, menu, double window, etc) that you wish to
adjust. Where will it all end?