I thought that fixing Mr Hilda’s JVC HR-D750EA VCR would be
relatively simple. His story was that he went away on holidays and switched it
off when he left but when he came back, it wouldn’t switch on straight away.
Instead, he could only get it to work intermittently. Finally, it wouldn’t start
at all, giving only a "squeak" and then nothing.
I quizzed him further and established that he was trying to get
it to start by switching it off and on using the power point switch on the wall.
He wasn’t using the remote control or the power switch on the front of the VCR
for this job.
Sets Covered This Month
- JVC HR-D750EA VCR
- National TC1407 portable TV set
- National NV-H70A VCR
- Mitsubishi CT2584AS stereo TV
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To me, this all suggested that one or more electrolytic
capacitors had gone leaky in this now 10-year-old VCR, especially the start-up
capacitor (which ever one it was) in the switchmode power supply.
In this machine, the main section of the power supply
consists of a separate module in a metal cage, in the far righthand corner
of the chassis. The rest of the power supply is on the main circuit board and
consists mostly of IC regulators. My initial attention was drawn to a regulator
in the cage, which was fairly easy to remove due to good access to the printed
side of the board.
Fig.1: part of the switchmode power supply circuitry in the JVC HR-D750EA VCR. There were several problems that prevented the supply from starting.
The first thing I did was scrape off the liberal quantities of
corrosive brown goo that had been applied to both sides of the board. The
component side proved to be a bit of a nightmare as the parts were packed
tightly between various metal screens and heatsinks.
That done, I examined the service manual which is marked
"switing regurator". Anyway, there were two electrolytic capacitors on the
primary side of the switchmode transformer (T1) that looked like the suspects I
was seeking. These were C14 1μF 50V and C13 180μF 16V.
I could see that all the electrolytics had been replaced some
years previously but these two were now well and truly dried out due to their
proximity to the heatsinks. I fitted two new EXR 105°C capacitors, substituting
a 220μF unit for the 180μF capacitor and also increasing the working
voltage of both values. The new capacitors were smaller than the originals so
this was straightforward.
By the way, the EXR range of electrolytic capacitors is
specially designed for high-frequency switchmode power supplies. They have very
low impedance and low leakage, typically around 4μA, which should give extra
long life.
The equivalent (effective) series resistance, or ESR, of an
electrolytic capacitor defines its performance and life; the lower it is, the
better the capacitor. An Australian engineer, Bob Parker, has designed an ESR
meter kit (available from Dick Smith Electronics, Cat.K-7204) to measure this.
Having just bought and built one of these, I was itching to give it a go.
The two capacitors I had taken out both measured high
impedance, the 180μF unit reading 44Ω and the 1μF unit not
reading at all. I had fitted an additional buzzer circuit, designed by Mark
Stevenson, that gives an audible sound if the capacitor is OK (ie, below
1Ω)
and a slight noise if it is less than 10Ω.
While I was at it, I measured all the remaining
electrolytics in-circuit with the ESR meter and the buzzer indicated that
they were OK, with two or three giving the lesser noise, (ie, possibly
borderline). I then resoldered any suspicious joints before putting it all back
together and switching it on, confident that it would work.
To my surprise, nothing happened. However, I was still
convinced it was really an electrolytic capacitor that was at fault, so I
replaced the three units that had given a doubtful reading on the ESR meter.
That didn’t fix it either.
Finally, I took the advice of a colleague who always
maintained that it was quicker and more reliable to just change the lot at
one go. I did this, replacing all 11 of them, and bombed out again!
Next, I checked the high value resistors R2, R3, R4, R7, R8 but
still no joy. I then checked the secondary output rails for shorts and was
finally rewarded by finding that D25, a 39V zener, was short circuit. But this
still did not fix the fault. To make matters worse, I then introduced a red
herring by unplugging the power supply from the VCR (in case the load was too
much).
This time the power supply finally fired up and I had
voltages on all the rails. However, when I plugged it back into the VCR, it
died again and so I checked for shorts on the main VCR rails. Again, nothing was
found – this sorry tale was just too frustrating but worse was to come. I
reconnected the two plugs while the power supply was on – fairly risky, I know,
but I was desperate – and the whole video burst into life!
I checked all the functions and apart from lines across the
screen in playback mode, everything worked fine, including the power on/off on
the set. But when I switched it off at the power point and then back on, it was
dead again!
By now I was feeling considerably older – I think my own
electrolytics were past their use-by date! The only thing left I hadn’t tried
was IC1 (STR1006), which I really doubted could be the problem – but naturally
it was. It only has three transistors, one zener and three resistors but it
was the culprit. My theory is that the two original electrolytics failed,
causing the output voltages to rise. And this in turn destroyed D25 and,
presumably, the zener diode in IC1.
But I still wasn’t out of the woods – I still had the lines on
playback, although they slowly weakened, the longer the set was on. From
experience these are also usually caused by faulty electrolytic capacitors, this
time on the 5V and 12V rails feeding the head amplifier. As a result, I
checked C802 to C807 with the ESR meter and they all checked OK. The ESR meter
makes it so much quicker, as they can be checked in-circuit and the meter was
proving to be very accurate.
It was then that I remembered a previous repair I had done on a
JVC HR-D400EA with the same fault. After a long saga, the fault had been traced
to the underside of a small soldered metal shield on the main video board. This
shield conceals a patch of brown goo which holds a 1kΩ resistor between pins 1 and
32 of IC102 (pin 3 being +5V Vcc and pin 1 9V Vss (PB12V) for the MS6967RS 1H
delay).
As before, removing the goo and corrosion also removed the
final problem. However, my persistence with this job had been a little
uneconomic and I really should have drawn the line sooner. I was, however, very
impressed with the ESR meter and can recommend it to you – good one,
Bob!
National TV set
My next story involves a complete change of scene. The local
motel brought in a National portable TV set, complaining of horizontal white
lines across the picture but only on Channel 7.
I wasn’t all that keen about repairing such an old (1984)
chassis – a TC1407 (M12H) – but was intrigued by the symptoms. Initially, I
suspected the CATV (cable antenna television system) antenna used in the motel
but when I connected my own antenna to the set, the same fault occurred. When I
tuned to Channel 7 there were bright white horizontal retrace lines about two
thirds the way down the screen from the top.
Because it was only on Channel 7, I reasoned that this was
because this is the only channel transmitting Teletext during the vertical
flyback interval.
The motel owner, while appreciating that the set was over 15
years old, was prepared to pay up to $100 to get it fixed. Apart from its
current problem, the set produced a good picture and had been very reliable.
Well, how difficult could it be to find a vertical blanking
fault? Surely this would be an easy $100, I foolishly told myself. In fact,
I still had an original service manual for this set, although the circuit
diagram is a bit of a mess and difficult to follow.
I discounted the AGC and IF stages and concentrated my efforts
on the blanking circuit between IC401 (the vertical output IC, AN5521), IC601
(the chroma decoder IC, AN5625) and IC301 (the video output IC, AN5615). By
using an oscilloscope, I thought that it wouldn’t take long too find out where
the blanking pulses disappeared. My assumption was that it was probably a
leaky electrolytic capacitor somewhere that was causing the problem.
I started at pin 6 of the vertical output IC (IC401) and
measured waveform 20, which is a 28V peak-to-peak vertical pulse (the DC value
being 0.3V). This turned out to be spot on. This pulse then goes through C416
and R424 where it joins the horizontal blanking pulse from pin 2 of the
horizontal output transformer via R553, C650, R678, R642 and D601.
The horizontal waveform (waveform 37) started out at 30V
peak-to-peak on pin 2 and is reduced to about 9V on the anode of D601 but no
information on the waveform at this point is supplied in the service manual.
However, the 5ms vertical pulse, embedded between the horizontal pulses, was
clearly visible.
Because I was expecting something dramatic, I was rather
perplexed to find that this waveform reached pin 18 of IC601 and pin 11 of IC301
quite correctly. This waveform (24) shows the horizontal pulse as 6.2V p-p,
which was spot on at a DC voltage of 1.2V. The vertical pulse was still there
too, so where was the obvious fault?
In my notes of previous repairs, I had recorded that a TC1408
(M12C) had displayed the same symptoms due to a faulty AN5615 (IC301). I now
felt sure this must also be the culprit here so I changed IC301, then IC601 and
then IC401 – all without result. Clutching at straws, I then replaced C414,
C416, C420 and C650. This made no difference either, so I measured the resistors
and diodes in circuit and all read OK.
By now I was really frustrated – by rights, I should have fixed
this supposedly simple fault and moved onto another job. Unfortunately, I still
didn’t have a clue but I was determined that it wasn’t going to beat me.
My next theory was that perhaps it was the width of the
vertical pulse that was the significant factor. An hour later I abandoned this
idea in a bad temper, even though I could vary the number of retrace lines by
carefully adjusting the vertical hold. I even changed IC501, the jungle IC
(AN5435) but the retrace lines were still visible on Channel 7.
In the past, I have had similar symptoms due to poor smoothing
of the 198V rail to the RGB outputs so I replaced C556 (10μF 250V). When
that didn’t work, I checked the screen volts but I was getting nowhere fast.
I had obviously overlooked something but I couldn’t think what
it was. All I could do now was go back over what I had done and recheck my
work.
A previous fault I had encountered with another set with no
colour had turned out to be a leaky diode (D602) which had distorted the
horizontal pulses to the burst gate. I remembered that, at the time, I couldn’t
measure this in-circuit to determine its leakage.
Therefore, I felt it would be a good idea to measure D402, D601
and D602 out of circuit with the ohmmeter on the 100kΩ range. And it was when I
measured D601 that I found the answer – there was significant reverse leakage.
Replacing it with a 1N4148 fixed the fault and the vertical pulse on its cathode
was double what it was previously.
I richly deserved the $100 I charged for this job but when will
I ever learn?
National NV-H70A VCR
Mr Peterson’s ageing National NV-H70A VCR came into the
workshop with the complaint that a tape was stuck inside. He neglected to
mention that the set was otherwise dead but on removing the covers the cause was
fairly obvious. F1102, a 2A fuse, was open circuit on the UNREG 18V rail that
also supplies several other rails: 12V, 7.2V, 6V and 5V. Replacing the fuse
restored all functions and I could do whatever I wanted with the tape.
Next, the phone rang and I had to deal with an enquiry that
took some time. Suddenly, towards the end of the conversation, I began to smell
burning.
Fig.2: this circuit section for the National NV-G30 proved to an effective substitute for a National NV-H70A. In particular, it allowed me to identify transistors Q6005 and Q6006, both of which had been "cooked".
I wound up the call as fast as I could and started sniffing
around for the source. And when there is a lot of electrical gear spread out and
all switched on, it can be hard to trace the source of a smell. Fortunately it
didn’t take long to trace this one; it was coming from Mr Peterson’s VCR!
Although it had been doing all its tricks minutes earlier, the
tape was now firmly stuck inside and wouldn’t budge. Sniffing carefully, I
traced the smell to two transistors on the righthand side of the
motherboard. These had become so hot that they had unsoldered themselves
and fallen out of the PC board so that they were now resting on the bottom of
the cabinet (the PC board is horizontal, with the wiring pattern on the top and
the components underneath).
Pretty neat trick, I thought – at least I wouldn’t have to
unsolder them. But that was the easy part. After scooping them up, I was faced
with the problem of identifying them; they had been carbonised and I didn’t have
a circuit diagram.
My approach was to find a similar National Panasonic
circuit – one with the same microprocessor chip set used on the main CBA
(Circuit Board Assembly VEP03309). That way, I would have a good chance of
identifying the transistors used.
The best substitute circuit I could find was for the NV-G30
model. The clue was IC6001, an MN15342VEB, which is used in both units. And the
transistors in this part of the NV-G30 circuit, Q6005 and Q6006, turned out to
be 2SB790s, which are general-purpose PNP transistors.
Before replacing these, I checked the circuit board for burn
marks. The two transistors are controlled by the microprocessor, with Q6006
switching a regulated +12V rail via the Record Safety Switch and Q6005 driven by
pin 43 D-REC (Delayed Record). Similarly, Q6008 is driven by pin 42 DA-REC
(Delayed Audio Record).
Apart from the two transistors there was no other apparent
damage so why did they get so hot and fail? This wasn’t easy to deduce but with
the common denominator being the regulated 12.3V supply, the source of the
problem had to be in the power supply itself.
Access to the power supply is not easy, with a lot of short
leads and metalwork in the way. Once it was out, I decided to adopt a blanket
approach and replace all 10 electrolytics with EXR 105° types. It was a fiddly
job but most of the capacitors looked pretty sorry anyway, especially C1101,
C1107 and C1104. Finally, I left it on soak test and I’m pleased to report that
there were no more pyrotechnics.
Mr Peterson is once again a happy man though I did advise
him to get a new one if it played up again. He would be surprised how cheap they
are now compared with what he paid some 13 years ago.
Mitsubishi stereo TV
Mr Crane requested a service call for his 1992 59cm Mitsubishi
CT2584AS (ASV59S/AS2 stereo chassis), which he said had an intermittent crackle
in the sound.
Initially, I was emphatic that an intermittent fault would have
to be fixed in the workshop but he was equally emphatic that it really wasn’t
intermittent and that because he was 76 years old, he couldn’t possibly get it
down the stairs of his duplex and into his car to deliver it to me. I saw his
point and relented.
When I arrived the next afternoon, I switched it on and sure
enough, there was a faint crackle on all channels. He assured me that it was
normally a lot louder. I knew I was going to regret it later but I decided to
take a quick look anyway, in the hope that I could fix it on the spot.
I pulled the set away from the wall, removed the back and
started tapping around, looking for a dry joint or a bad connection. After a few
minutes, I emerged from behind the set having achieved nothing except that when
I looked at the picture it was line tearing. "Oh yes", said Mr Crane, "it does
that too sometimes". I secretly sighed with relief – I hated to think I might
have been held responsible for this "new" problem. "Well", I said
authoritatively, "that settles that, I will have to take it back to the
workshop". I lent him a portable set and with immense difficulty finally got his
set into the car and back to the workshop.
The set must have enjoyed the ride because when I switched it
on, all the faults had cleared and the picture was excellent. Such is life, I
thought and left it to soak test. The crackling in the sound refused to come
back but the line tearing did occasionally.
I took the chassis out and reworked the soldering for any
potential dry joints – there were none that were significant. I also noticed
that the heatshrink tubing on some of the electrolytics had peeled back.
Initially, I replaced three capacitors in the power supply secondary – C917 and
C453 on the 28V rail to the vertical output IC (IC451) and C920 on the 15V input
to the two 12V regulators (IC902 & IC103). I also replaced C552
(1μF
160V) which connects to the line driver Q551/T552.
The two significant capacitors were C917 and C920 as they smelt
"fishy" when I unsoldered them. They had spilt their electrolyte and this had
attacked the copper tracks on the board. Anyway, this finally fixed the line
tearing but I didn’t know what to do about the sound.
I left it on soak test for another two weeks before Mr Crane
finally demanded I return it. Reluctantly, I agreed but didn’t have much faith
in the long-term reliability of the set and told him so.
The set bounces
As I expected, Mr Crane was back on the phone just two months
later to let me know that didn’t last long. And despite my previous
explanations, he seemed to think that it was all my fault (which I also
expected).
I called the next afternoon and listened attentively to the
elusive crackle. This time I established that it wasn’t due to interference from
an external source. Instead, it sounded as though it was due to arcing somewhere
inside the set. With the speakers switched off I couldn’t hear it at all but I
thought it might have been arcing internally inside the flyback transformer or
even the deflection yoke and that the interference was finding its way into the
audio chain.
I disconnected the yoke momentarily and it wasn’t that. I also
unplugged the CRT socket in case it was arcing inside the tube guns but it
wasn’t from that either. Finally, I decided that it was the flyback transformer
that was the cause of the problem and told Mr Crane that it would be expensive
to replace. It was time now for him to put up or shut up. He decided to invest
in a new transformer.
It took the set back to the workshop to wait for a new flyback
transformer. And although I had sounded confident, it was really only an
intelligent guess. I knew that if this didn’t fix it, I would have to keep at it
until I had cracked it.
Finally the new part arrived. I unsoldered the old one using a
solder sucker but I ran into problems when I tried to remove the EHT final
anode/ultor cap to the tube. The type of rubber that Mitsubishi uses is quite
hard and resilient compared to others and getting a screwdriver underneath it
was difficult. Then I had to push in the side clips that hold it on to the tube
before one side came away and I finally got it off.
The reason I had problems removing it was that it was extremely
rusty underneath, with heaps of fine brown-red rust powder everywhere. This
mystified me, as there was absolutely no sign of rust or water damage anywhere
else but it got me thinking – was this the cause of the invisible arcing and
crackling in the sound?
I cleaned up the rust with a wire brush and CRC 2-26 and fitted
the new flyback transformer – I didn’t have the time or patience to refit the
old one and because of the intermittent nature of the fault, I felt that the
result would have been inconclusive.
As additional insurance, I replaced all the electrolytics
feeding the audio output stages and reworked the sound module. Once again I soak
tested the set before returning it to an anxious Mr Crane. It is now over three
months since it went back so I feel confident that it has really been fixed.