When the first batch of imported colour TV sets hit the
Australian market in March 1975, there was fierce competition between the local
brands (HMV, Healing, Pye, Philips, Kriesler) and those from the UK and Japan.
Indeed, there was a huge shake up as one outsider, Rank Arena (a UK/Japanese
consortium), offered a modified NEC NTSC chassis which made major inroads into
the established market.
In addition, many new brands were either fully imported or
assembled from kits in brand new factories. There was also a lot of
rebadging.
National started with its M4 series which had plug-in modules
and was built in Penrith. Sharp had an 18-inch model which was a monster to
repair, while General produced a highly successful 14-inch portable before
moving into larger models later on. Hitachi and Sony also started off with good
portables. Most of the Japanese-derived sets were modified NTSC sets and were
built like battleships. Some of these sets are still working now, 25 years
later.
Sets Covered This Month
- Akai VS765 VCR.
- Toshiba Bazooka Model 3408H 80cm TV set.
- Teac MV1480MkII TV/VCR.
- Panasonic NV-HD100A VCR.
- Sharp VC-H85X Hifi VCR
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The locally-designed and built sets were based on European
designs which, although highly successful in their countries of origin, were not
so successful here – despite being significantly upgraded for Australian
standards.
AWA/Thorn started with a modified 3K5 chassis from the UK. In
the UK, they produced millions of these but out here they weren’t as reliable as
their Japanese counterparts. When AWA/Thorn subsequently started their
Mitsubishi-designed G and K chassis, I well remember a service technician
meeting at which the Mitsubishi Service Manager began by stating "Well,
Gentlemen, you will all soon be out of a job"!
He was wrong, of course, but from simple monochrome sets that
broke down up to three times a year, we have progressed to sets that we consider
poor if they break down once in three years. However, the quality of soldering
is as bad today as it was then and faulty joints are still very common. Yet, in
the computer industry, they are almost unheard of – no doubt due to the
widespread use of plated-though holes on the PC boards.
Fig.1: part of the DC-DC converter which supplies a -35V rail and a 4V rail in the Akai VS765 VCR. Transformer L404 is on the left and L405 to its right
The early video recorders used piano key controls and came with
a multiplicity of belts, tyres and rollers. As a result, they required a belt
kit replacement every few years. Nowadays, everything is microprocessor
controlled but the decks use flimsy plastic gears. Many faults these days are
due to customer abuse, to which a lot of modern equipment is much less
tolerant.
Those technicians who work with only one brand become very
quick at fixing them but often they miss the bigger picture. By contrast,
technicians who work on many brands are able to appreciate why some circuits are
more reliable than others and often substitute more rugged components or make
other modifications to troublesome circuits.
Modifications are also issued by the manufacturers but fitting
them to a set that is, say, over five years old is often unnecessary (unless
safety is involved). After all, if the set has lasted that long, the original
circuit could not have been all that bad.
Alternatively, there have been cases where the manufacturer has
produced modifications only to change them again and again. NEC did this with
the earlier series of Daewoo TV chassis, eventually issuing a chart of
modifications appropriate for a range of serial numbers within the same model
series.
Akai is very responsive to problems in their equipment and
their service agents are sent copies of service bulletins on all their products.
For example, in the SX series video recorders, from the late 80s/early 90s, they
were quick to pick up a problem with the fluorescent displays going dark or
failing altogether. This was due to the failure of two electrolytic capacitors
in the DC-to-DC converter which supplied a -35V rail.
Akai VS765 VCR
I had such a case recently involving one of the SX series, an
Akai VS765. Mrs Brady had brought it in with the classic no display fault. The
voltages on the fluoro segments were very low, with the normal -35V supply from
plug WP1-1 down to about half its correct value. Replacing the usual culprits –
C446 and C447 – with 100μF 25V capacitors restored the voltage but not the
display.
When I measured the display’s filaments, I found that there was
continuity but no 4V across them. Once again, it was back to the weird little
DC-DC converter Akai is so fond of. I checked D416 and D417 and also the
secondary track for cracks but everything looked OK. By this stage, I was rather
puzzled as it was hard to understand why the -35V rail was OK but not the 4V
rail.
I subsequently wasted a lot of time chasing red herrings, such
as replacing D416 and D417 with RB-100AT types and fitting a 2.2Ω 0.5W resistor in series
with C447. I also wasted a lot of time checking all the other supply rails and
the fluorescent display itself out of circuit, but was getting nowhere.
In desperation, I started pulling out each component, testing
it and replacing it. As always, these parts are the most difficult to reach and
I confess that I acquired a lot of pleasure from cutting out a piece of plastic
from the main case underneath the bottom cover (where it wouldn’t be noticed) to
provide better access to the PC board.
Finally, my agony was over when I removed transformer L404 and
found that its primary was open circuit – due to corrosion from our favourite
brown goo inside the can. The reason I couldn’t measure it previously in circuit
was because L405, a 1.8mH choke, is in parallel with it, masking the fault. A
new transformer restored the fluorescent display and my
sanity.
Good news & bad
The Strathfields had good news and bad news. The bad news was
that they had an 80cm Toshiba TV set that needed fixing. The good news was that
it was a height/linearity problem, a fault that I’m quite familiar with. More
specifically, there are two brightly coloured 2.2μF electros that spill their insides in
many Toshiba sets and cause this problem.
This job entailed a house call to attend the Toshiba monster,
appropriately called the "Bazooka" (no kidding) Model No. 3408H. I didn’t have a
service manual but I felt that this would be in the bag within half an hour.
Silly me!
The set was sensibly placed in a large rumpus room with good
access and lighting. I switched it on and confirmed the fault. I had brought
along a small army of electrolytic capacitors because some models use different
values.
Everything was looking good, although the chassis was
unfamiliar compared with anything I had seen before. Now all I had to do was
find the two culprits which should be designated C303 (1μF) and C317 (2.2μF) in small but different coloured
heatshrink plastic cases. The former should be near pin 31 of the large 64-pin
jungle IC (IC501, TA8659N). The latter should be near the vertical output stage
(pin 2 of IC303, AN5521).
I found C317 fairly quickly, although its heatshrink colour was
dark brown or black, which doesn’t stand out as well as in previous models.
Anyway, I was half-way there. All I had to do was find C303 and replace it but
this was where I came unstuck. Though IC501 was a 64-pin jungle IC, it was now a
TA8783N and pin 31 was not connected! Furthermore, an extra 16-pin IC,
designated IC371 (TA-8739P), had been added and I had no idea what this device
was for!
It was also about this time that I was informed that the fault
was intermittent; that after it had been on for about 10 minutes it would often
come good and stay like that. This was not good news because how would I know
when it was fixed if it was intermittent?
By now I was becoming increasingly pessimistic that I could fix
this one on the spot. My guess was that Toshiba, in its wisdom, had scrubbed the
pin 31 function of IC502 and substituted IC371 instead, as part of and parcel of
some new system.
I fished out the freezer and started hitting the small electros
around IC371. Fortunately, I was rewarded immediately by all sorts of vertical
deflection activity, which suggested that I might be on the right track. I found
and replaced C374 (120μF 25V) and C372 (0.47μF). The latter in particular was leaky but this didn’t
completely fix the problem though it was a lot better and even Mrs Strathfield,
who was watching, was impressed.
As I was replacing the two previous capacitors, I noticed a
2.2μF
electrolytic, underneath the IC, on the copper side of the board, between pins 3
and 15. This had apparently been changed during production at the factory from
its drilled and punched position, marked C372, to where it was now. When I
removed it, I also noticed that its insides had spilt onto one of the copper
tracks and corroded it.
Cleaning it all up, repairing the corroded copper and replacing
this capacitor finally fixed the fault.
Naturally, I was relieved that I managed to get that problem
sorted out in situ, as no doubt was Mrs Strathfield. At the same time, due to
the intermittent nature of the original fault, I was concerned that it might
recur in the weeks and months to follow. Fortunately it didn’t bounce and while
going through my Toshiba service manuals back at the workshop, I found a circuit
for similar models (3418DA/2529SM) which confirmed that I had done the right
thing.
Teac TV/VCR
My next story involves a Teac MV1480MkII TV/VCR combination
that arrived by courier with no note – not even a name and address and certainly
no fault marked. I waited a day or so to see if its owner would contact me but
no one did.
Anyway, when I had a moment I put it up on the bench and
switched it on. The set came on for a few moments and then switched itself off
(I could hear the click from the relay). However, while the set was on, the
picture and sound were both good.
I removed the back and the first thing to catch my eye was the
sheer volume of dust on the inside. After blowing it all out with the
compressor, I located the mains input and relay on a sub board, on the lefthand
side looking from the rear. Fortunately, I did have a service manual and I
established that the relay switched the AC power to the TV monitor section of
the set. I also established that there was no feedback from the separate
self-contained TV PC board that might contain some sort of safety circuit, nor
was any part of it used to power the VCR or relay circuits.
So I wasn’t looking for a fault in the TV set but rather in the
relay circuit or possibly the VCR.
The relay was controlled by two transistors, which required two
conditions to be met for it to switch on. First, the power switch had to tell
the VCR main microprocessor to switch on the relay. Second, the 12V rail had to
be there. Both these conditions were being met for a short while but
measurements soon indicated that both disappeared simultaneously after about
30-60 seconds.
For a while, I suspected that the two transistors might be
faulty and spent some time checking them. However, this seemed unlikely, as the
set switched on and off repeatedly in exactly the same manner which told me that
something else was instructing the microprocessor to turn the set off. This
wasn’t good news – access to the microprocessor is quite difficult and involves
removing the Funai VCR deck and all its boards.
I was about to do this when I noticed that a videocassette was
still inside the machine, so I tried to eject it. However, despite actually
making a lot of promising noises, it was unable to perform any function before
the set switched off. I really needed the tape out before I could disassemble
the machine, so I wound the cassette carriage ejector pulley by hand until it
was out.
I wasn’t sure what the loading motor would do now – after all,
the carriage was now up but the mode select switch would remember it as being
down. In view of this, I decided to power up the set to see what would happen. I
reasoned that it would be best to deal with any loading logic problems
immediately, before things got out of hand.
Fortunately, the VCR only gave a few whirring sounds from its
gears before settling down and stopping. There was hardly any major
movement.
The interesting thing was that the set now stayed on and was
still on five minutes later. Being rash, I decided to tease the VCR gods by
re-inserting the same tape and seeing if I could recreate the fault. But I
couldn’t make it misbehave – the set stayed on and the tape played
flawlessly.
So what actually happened? Well, it’s one of those boring old
stories I rarely write about – the belts were old and worn and prone to
slipping. The mechanism had jammed in no-man’s-land and the microprocessor had
switched the set off – elementary, my dear Watson. Strangely, the owner still
hasn’t phoned but I’m quoting for a new belt kit and a couple of hours
work.
Panasonic VCR
Some time ago, I reported on a Panasonic NV-HD100A VCR that had
noise on standard playback (SP) but was OK on long play (LP). I cleaned the
heads but that made no difference and finally diagnosed, located and repaired a
hairline fracture in the solder on pins 1, 2 and 3 of plug P502 of the head
amplifier. I discovered this by wobbling the head amplifier in situ until the
picture came good.
Resoldering the joints appeared to fix the problem because I
left it on soak test for days before the client picked it up and everything was
perfect. I didn’t think any more about it until just over three months later,
when the owner phoned to complain that it was doing the same thing again. It was
the same old routine emotive story that I’ve heard many times – the fault was
exactly same and they had hardly used it, etc, etc.
So why did they wait until it was out of warranty to report it?
I didn’t press the point and as my policy is to always give the customer the
benefit of the doubt, I told them to return the set and I would check it out.
They came in the next day and I checked it out in front of them, fully expecting
it to be some other symptom that they were not astute enough to identify.
My arrogance was quickly crushed when I discovered that it was
indeed exactly the same fault as before. Just in case, I removed the covers and
cleaned the heads and it was still crook. I then wiggled the head amplifier and
the fault came good. Well, these people had a point; I would have to investigate
further and they would have to leave it with me.
How could a resoldered faulty joint or fracture break again? It
definitely wasn’t possible and there had to be some other explanation.
I took the head amplifier out of the K chassis mechanism/deck
and examined it more carefully under a magnifying lamp. I was pleased to see
that there were definitely no more suspect joints but where to from here? The
head amplifier plugs into the lower head drum assembly PC board, which carries
the static coils of the rotary transformer. I hoped these weren’t open circuit –
being a hifi VCR, their cost would exceed the price of a new VCR. How would I
explain that?
Next, I removed the entire cylinder (upper and lower assembly),
after first removing the antistatic wiper and auto head cleaner on the top.
There are only three screws underneath to release the mechanism, plus the plugs
and sockets.
With the assembly upside down on the bench and with its cover
removed, I could now clearly see a row of suspect joints, especially along the
plug sockets. In fact, the entire board was poorly soldered and even the rotary
transformer winding terminations looked crook. I reworked the entire board very
carefully, then reassembled and tested the deck.
Once again everything was working properly and after soak
testing it, I returned the set to its owners at no charge.
That’s not all
I thought that that would be the end of this saga but they were
back on the phone just six weeks later. As before, they trotted out the familiar
routine, complaining that it was exactly the same fault as before, that the set
had never been right, etc, etc.
I cut them off at the pass by telling them that if they brought
it in, I would look at it straight away. Surely lightning couldn’t strike twice
at the same spot, I thought. They were around in the blink of an eye and
although they were icily polite, I sensed that something was different.
When I tested the machine, it turned out that the tape was
jamming inside. So much for their complaint that it was "doing the same thing as
before". I removed the cover and there, staring right back at all of us, was a
cassette label stuck over the idler in the centre at the bottom of cassette
carriage. I pulled it out with a pair of pliers and, without comment, passed it
to the more vocal of the pair. I then connected the VCR to a TV set, put in a
cassette, made a recording and played it back right in front of them.
Bashfully, they took their machine and, with tails between
their legs, made for the exit.
As a PS to this story, I have had similar faulty joint
experiences with this type of failure on two subsequent K chassis Panasonic
VCRs, so this may be a common problem.
Sharp hifi VCR
Mr Andriotti has no less than two Sharp VC-H85X hifi VCRs and
both were not only faulty but had the same fault. Because of this, he felt that
he should get a discount for bulk repairs but I felt the opposite. In the end,
we agreed that we would wait until I had diagnosed the fault(s).
He described the sets as "dead and whistling". The first one I
looked at was doing precisely that and the whistling was coming from the
switchmode power supply cage on the righthand side.
Removing the power supply from the rest of the VCR was
difficult as it is hard to get it past the top PC board. Eventually, my
persistence paid off and I finally got it onto the bench and removed its
covers.
The main suspect
It didn’t take long to identify a leaky 47μF 16V electrolytic (C913) as
the main suspect. Refitting the power supply into the VCR took longer than
replacing the capacitor but eventually it was back in and the set returned to
life. I checked all the functions and everything worked OK, except that rewind
was slow towards the end. I put this down to belts and decided that they should
be replaced, subject to haggling with Mr Andriotti.
I reached for the next VCR and plugged it in but it burst into
life immediately. I decided to look at the power supply anyway and C913 was even
more leaky that its sister in the first machine. I replaced it but when it came
to checking the set’s functions, it was worse than the previous one. I removed
the base cover to check the state of the reel idler belt and discovered that it
was worn. In addition, the capstan motor plastic pulley was cracked and
slipping.
Armed with these facts, I sought out Mr Andriotti and after
some light banter, we settled on an amicable deal which involved changing the
belts and tyres and gluing the pulley. As it happened, when I checked the first
VCR, the same plastic pulley was also cracked.
By the way, I am fairly certain that this pulley is now
available as a spare part, although it is not in the service manual except as
part of the capstan motor assembly. It’s possible that the replacement is
similar to the Mitsubishi one – a brass pulley which costs an arm and a leg.
Gluing it seemed to be the cheapest way.